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Well ID: 34-169-23544 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wayne | |
Municipality: Baughman Township | |
Operator Name: H A D INC | |
Well Pad ID: | |
Farm/Lease Name: WERTZ | |
License Status: Final Restoration | |
License Date: 1983-03-29 | |
Spud Date: 1983-03-31 | |
Spud Drilling Contractor: CO TOOLS | |
Final Drill Date: 1983-06-10 | |
Well Total Depth: 2990.00 ft | |
Configuration: Vertical | |
Latitude: 40.890000 | |
Longitude: -81.680000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1983-03-29 | 381 H A D INC GeoDate 3/29/83 |
Oil and Gas | 1983-03-29 | Issued Date 3/29/83 Expired Date 9/25/83 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 02990 Proposed Drill Depth 02990 |
Original Spud | 1983-03-31 | |
Completed | 1983-06-10 | |
Plugged/Abandoned | 1983-06-10 | |
Reached Total Depth | 1983-06-10 | |
Completion Report Received | 1983-08-04 | |
Construction Permit Expires | 1983-09-25 | |
Record Last Modified | 2013-03-14 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | LOST HOLE @ 2560 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-983649639 | 2005-6-23 0:00: | PB | No Violations | 1.50 |
0000DP9849 | Final Restoration | No Violations | Final Restoration done information from Data Point | |
0983649639 | 2005-06-23 | Plug / Plug Back | No Violations | Check on plug rig and found that they will not be ready today and that job will be moved back until Thursday. |
1045762634 | 2005-06-28 | Plug / Plug Back | No Violations | During plugging of perfs it was discovered that the casing had a hole in it.It was discovered after cement was mixed and displaced .It was agreed that the casing would have to be drilled out and most likely shot off because there was cement on the back si |
1291340534 | 2005-06-30 | Plug / Plug Back | No Violations | Check on plug depth and also check for leaks.Found cement at surface with no leaks.Rig moving off today. |
1299065224 | 2005-06-29 | Plug / Plug Back | No Violations | Shot casing at 2150 ft with 30 ft. spread and set 200 ft. Lime plug.Then pull tubing and try and rip casing to set remaining plugs.Found out they could not rip casing and had to call the shooters back out and did shoot it off at 700 ft. then set remainin |
DP9849 | FR | No Violations |
For data sources see[4]