X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-169-25134

Well Details

Well ID: 34-169-25134
Loading map...
Country: United States
State: Ohio
County: Wayne
Municipality: Milton Township
Operator Name: MORTON SALT INC
Well Pad ID:
Farm/Lease Name: MORTON SALT {SMP # 4}
License Status: Final Restoration
License Date: 2009-09-09
Spud Date: 2009-10-13
Spud Drilling Contractor: IPSCO
Final Drill Date: 1996-12-10
Well Total Depth: 5451.00 ft
Configuration: Horizontal
Latitude: 40.950000
Longitude: -81.810000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1996-10-09 3509 MORTON SALT/MORTON INTL GeoDate 10/9/96
Solution Mining 1996-10-09 Issued Date 10/9/96 Expired Date 10/9/97 Acres 0000000 Tool Type RTAF Proposed Formation SALINA Proposed Depth 02580 Proposed Drill Depth 02580
Original Spud 1996-11-20 CHG LOC/XY/ELEV 1-25-97
Completed 1996-12-10 CHG LOC/XY/ELEV 1-25-97
Reached Total Depth 1996-12-10 CHG LOC/XY/ELEV 1-25-97
Annulus Pressure Monitoring Approved 1997-01-07 CHG LOC/XY/ELEV 1-25-97
Completion Report Received 1997-01-09 CHG LOC/XY/ELEV 1-25-97
Last Compliance Report 2002-07-02 CHG LOC/XY/ELEV 1-25-97
APP 2008-06-16 Proposed Formations:SALINA, Issued Date:6/16/2008, Expired Date:6/16/2009 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class:SMP
APP 2009-09-09 Proposed Formations:SALINA, Issued Date:9/9/2009, Expired Date:9/9/2010 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class:SMP
Plugged/Abandoned 2009-10-14 CHG LOC/XY/ELEV 1-25-97
Construction Permit Expires 2010-09-09 CHG LOC/XY/ELEV 1-25-97
Change of Owner 2010-11-29 Operator changed from 3509, MORTON SALT INC to 8736, MORTON SALT INC
Record Last Modified 2017-02-15 CHG LOC/XY/ELEV 1-25-97

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1999-09-13 2475 2545 0
2475 2545 0
2475 2545 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NONE

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1006248498 2013-3-22 0:00: FR No Violations 0.50
-1309840519 2007-9-5 0:00:0 SM No Violations 1.20
-1756215711 2010-3-9 0:00:0 SM No Violations 1.00
-2062499377 2007-9-5 0:00:0 SM No Violations 1.20
-2069936020 2003-12-9 0:00: SM No Violations
-260570545 2007-9-26 0:00: SM No Violations 1.50
-65313807 2007-9-12 0:00: SM No Violations 8.00
0029376108 2002-05-23 Solution Mining Project No Violations Test M.I.T. for 5 year review for U.I.C. Test passed.
0065313807 2007-09-12 Solution Mining Project No Violations Arrive for MIT and test has failed and is to be retested soon.
0260570545 2007-09-26 Solution Mining Project No Violations Arrive today for M.I.T and found that they had forgot to call me to tell me the test will be Wednesday.
0268370907 2007-09-28 Solution Mining Project No Violations Arrive for M.I.T. and after 6 hrs test was cancelled due to mechanical problems with equipment.
0458436064 2009-10-13 Plug / Plug Back No Violations Whipstock Service company had Superior Wire line set 9 5/8 bridgeplug at 2332 on 10/12/2009 which was a Holiday for us so I did not witness .The 5 1/2 tubing has been pulled from 2350 ft and the last joint was bent and smashed which could be from cave in at that depth.Next load 9 5/8 casing and try and pressure test bridgeplug.3 tests failed .Then had Halliburton set cement plug on top of bridge and shut in for the night.Set 500 ft plug c/w 165 sks from 2332 to 1832 ft.
0565827411 2010-12-10 Final Restoration No Violations Check this well for Erica Freeman and found that it was plugged but needs marker plate with the correct info valves removed before final can be approved. Met with operator and advised that the well be capped with proper permit info and valves be removed.
0784562530 2009-10-19 Solution Mining Project No Violations Check on top of cement and found that it is down 3 ft and there are no leaks at this time.
1006248498 2013-03-22 Final Restoration No Violations Appears to be in compliance.
1193313116 2007-09-10 Solution Mining Project No Violations Arrive for M.I.T. and found that it has been cancelled until Weds.
1226151984 2007-09-12 Solution Mining Project No Violations Test M.I.T today and in the 7 hour the test failed and was stopped by operator. Use well # 41 as reference well.
1309840519 2007-09-05 Solution Mining Project No Violations Check this well to see if operator is pumping interface for M.I.T and did not find anybody in the well field to find out if the test is going to be soon.
1378343061 2007-09-10 Solution Mining Project No Violations Arrive for M.I.T. today and found they had forgot to call and reshcedule for this Weds.
1401406901 2007-10-11 Solution Mining Project No Violations Check well today and found no work done to get wells ready to test for M.I.T.
1451889015 2009-10-14 Plug / Plug Back No Violations Arrive for test after setting cement plug and tests # 1 & 2 failed because swedge was leaking. Make repairs and 3 rd test passed.Tag top of cement at 1812 ft . Halliburton set 2 plug from 1800 to 1500 then continue from 1500 to 1000 - 1000 to 500 and 500 to 0 ft. Need to top off as we ran out just as cement circulated to top and fell back several feet.
1645316472 2007-10-10 Solution Mining Project No Violations Check to see if wells are being worked on today and found that nothing has been done.
1669574741 2010-04-06 Final Restoration No Violations Final Restoration has not been done.
1756215711 2010-03-09 Solution Mining Project No Violations Pits are closed and area needs graded and seeded .Final not ready
2004812552 2010-06-16 Final Restoration No Violations Check on restoration final and found that it is not ready. The plate for top of the well does not have the correct info and there are production valves which need removed.
2062499377 2007-09-05 Solution Mining Project No Violations Morton Salt is pumping interface for MIT on Thurs or Fri
2069936020 2003-12-09 Solution Mining Project No Violations CHECKED ID - OK
2079472919 2007-09-28 Solution Mining Project No Violations Arrive to test M.I.T. and after 7 hours test was stopped.Had leak between tubing and valve.
268370907 2007-9-28 0:00: SM No Violations 8.00
29376108 2002-5-23 0:00: SM No Violations 10.50
458436064 2009-10-13 0:00 PB No Violations 9.00
565827411 2010-12-10 0:00 FR No Violations 0.70
784562530 2009-10-19 0:00 SM No Violations 1.00
iANGE00015 1997-08-01 Preliminary Restoration No Violations
iANGE000153 1997-8-1 0:00:0 PL No Violations

For data sources see[5]

References