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Well ID: 34-173-20575 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wood | |
Municipality: Portage Township | |
Operator Name: OHIO ENERGY OPERATORS LLC | |
Well Pad ID: | |
Farm/Lease Name: DOVE | |
License Status: Well Drilled | |
License Date: 2018-01-19 | |
Spud Date: 2011-01-19 | |
Spud Drilling Contractor: ADVANCED ENERGY SERVICES LLC | |
Final Drill Date: 2011-01-22 | |
Well Total Depth: 1310.00 ft | |
Configuration: Vertical | |
Latitude: 41.290000 | |
Longitude: -83.630000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2010-12-29 | Proposed Formations:TRENTON, Issued Date:10/1/2013, Expired Date:10/1/2015 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2011-01-22 | |
Correction to Well | 2013-10-04 | CORRECTION TO PERMIT NUMBER |
Change of Owner | 2015-01-27 | Operator changed from 8750, WESTERN NATURAL RES OP LLC to 9423, OHIO ENERGY OPERATORS LLC |
Completion Report Received | 2016-03-15 | |
APP | 2018-01-19 | Proposed Formations:TRENTON, Issued Date:1/19/2018, Expired Date:1/19/2020 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL |
Record Last Modified | 2018-01-26 | |
Construction Permit Expires | 2020-01-19 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2015-08-20 | 1144 | 0 | |
1144 | 0 | ||
1144 | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1067157230 | 2011-2-8 0:00:0 | PW | No Violations | |
-109653811 | 2012-9-20 0:00: | PW | No Violations | |
-1493735213 | 2017-12-26 0:00 | PW | No Violations | |
-1717378990 | 2011-10-11 0:00 | PW | No Violations | |
-2123006190 | 2016-3-28 0:00: | PL | No Violations | |
-2146757917 | 2019-12-10 0:00 | PW | No Violations | |
-297037516 | 2015-8-12 0:00: | PW | No Violations | |
-716238176 | 2018-3-19 0:00: | PW | No Violations | |
0109653811 | 2012-09-20 | Production Wells | No Violations | At the time of my inspection the well was shut in with the power disconnected. There was 50 psi on the annulus and 15 psi on the production line. There was also no identification posted at the well or the tank battery. I am waiting for a response from the operator or the landowner regarding the status of the well. |
0154506501 | 2015-08-14 | Plug / Plug Back | No Violations | Owner decide to plug back well from the Trenton formation to the Clinton equivalent. Petroset from Wooster Ohio was the cement contractor on site. One hundred sacks of Class A cement were used for the plugging program. Cement did not circulate to surface and was found to exist at 45 inches from surface. Owner used ready mix cement to fill casing to surface. |
0297037516 | 2015-08-12 | Production Wells | No Violations | Inspect well. The operator conducted cement bond log to evaluate well condition to perforate and produce the Clinton Formation equivelant from 462 feet to 458 feet. The cement bond log was performed by Jet Wireline Services, Inc. The top of cement for the 5.5 inch casing was determined to be at 480 feet below grade. The determination was made to squeeze cement in the annulus. A bridge plug set at 520 feet and the 5.5 inch casing was perforated at 485 feet to 487 feet with 9 shots. Communications between casings. |
0367055509 | 2011-03-03 | Drill / Deepen / Reopen | No Violations | Inspect drill site. Pipe has been run and cemented. |
0716238176 | 2018-03-19 | Production Wells | No Violations | Jet wireline on site to perforate the Trenton Formation. |
1016093949 | 2017-07-13 | Production Wells | No Violations | Well currently has a small pump jack with an electric motor installed. Well was plug back to a depth of 480 feet in 2015 and owner is currently testing well after plug back procedure. Identification is posted at site and well is currently producing into multiple tanks in a central location. Tank area include four 210 Bbl. structures and inside dike area has a slight skim of oil from a tank overflowing. Operator is in the process of cleanup at this site. No brine or oil was released because of the overflow. |
1067157230 | 2011-02-08 | Production Wells | No Violations | Inspect well. Berry Well service is going to run 4.5 inch pipe on well. |
1394223086 | 2014-02-21 | Production Wells | No Violations | At the time of the inspection the well was cabable of production but not currently producing. The operator, Western Natural Res Op LLC, has gone bankrupt and the well was sold to the landowner in a Sherrifs Auction. The landowner, Mr. Carpenter, is looking to have another operator take over the wells and the lease. The well is not to be produced until a properly registered/insured operator obtains the well. |
1429110820 | 2015-04-15 | Production Wells | No Violations | At the time of inspection, the well is capable of production and identification is posted at location. |
1441960211 | 2012-11-27 | Production Wells | No Violations | At the time of my inspection the well was capable of production but shut in and not currently in production. There was no identification posted and no change from the previous inspection. |
1493735213 | 2017-12-26 | Production Wells | No Violations | Well was recently reworked and half tank is still on site. Replaced gas powered pump jack with electric powered pump jack. Identification is posted and no observed violations at the present time. |
1516124360 | 2018-01-16 | Production Wells | No Violations | Spoke with owner of Ohio Energy Operators LLC about Chiefs Order # 2018-7. I explained that order was issued for lack of liability insurance. Inspected well and well is currently not in production. Advised owner to contact the Central Office of the Oil and Gas division of ODNR and to cease any production or service work on this well until liability insurance is obtained. Inspected tank area and found broken flow valve dumping liquid in dike area. Contacted pumper for this well and he responded and repaired the valve. |
1516818665 | 2018-01-24 | Production Wells | No Violations | Checked the progress of the clean up of the fluid inside of dike area. Last week, flow valve malfunctioned and allowed fluid to enter dike area. Cleanup appears to be about 90% completed and cleanup will continue when weather allows. |
1521633041 | 2018-03-19 | Production Wells | No Violations | On site to observe the logging and the operation of adding additional perforations to this well. |
1542650455 | 2018-11-19 | Production Wells | No Violations | Well currently does not have a pumpjack on. Spoke with operator and he is waiting on a submersible pump to install. Identification is posted at the well site. |
154506501 | 2015-8-14 0:00: | PB | No Violations | |
1717378990 | 2011-10-11 | Production Wells | No Violations | Well set to produce and work currently being done on tank battery and production lines. Frac tanks removed from site. ID needs posted. |
1724171086 | 2017-08-23 | Production Wells | No Violations | Identification has been recently updated and no observed violations at the present time. |
1743923868 | 2011-12-02 | Preliminary Restoration | No Violations | Pits filled and area graded for farm use. Well in production. Preliminary Restoration Passed. ID needs posted. Talked with operator who indicates signs have been ordered and will be posted promptly. |
1768675954 | 2011-07-05 | Production Wells | No Violations | Well capable of producing but needs preliminary restoration. Three frac type tanks located 20north of well and a water well located 20 to south of well. Submersible pump set on 2 3/8 upset tubing. Portable generator on site to power the pump. Tank Battery under construction. Lane access off Mermill Rd. |
1849917771 | 2018-04-11 | Production Wells | No Violations | A water sample was collected for analysis. The specific gravity was field tested at 1.05 units. |
2123006190 | 2016-03-28 | Preliminary Restoration | No Violations | Preliminary restoration has been completed. Small Churchill pump jack installed on well with gasoline engine. Identification is posted. |
367055509 | 2011-3-3 0:00:0 | DD | No Violations |
For data sources see[4]