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37-003-22239

Well Details

Well ID: 37-003-22239
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Country: United States
State: Pennsylvania
County: Allegheny
Municipality: Richland Township
Operator Name: UNKNOWN OPR
Well Pad ID:
Farm/Lease Name: Pittsburgh Cut Flowers
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: COMB. OIL&GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.657333
Longitude: -79.984833

For data sources see[1][2][3]

Well History

Date Event
2018-05-23 Begin Plugging
2018-06-01 Finished Plugging
2019-06-26 Fully Plugged

For data sources see[4]



Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2460904 Primary Facility 2016-03-03 Routine/Complete Inspection No Adverse Event or Action Reported Well intact, complete w/ pumpjack (without power unit), rods & tubing. Small gas leak @ wellhead, no noticeable oil leaks. All lines disconnected and capped. No tank.
2479562 Primary Facility 2016-04-26 Routine/Partial Inspection No Adverse Event or Action Reported Met with Richland Twp. representatives & a partner in the development planned for the property to inspect the wellsite and discuss details of filing for CFA grant to plug the well.
2479564 Primary Facility 2016-04-25 Routine/Partial Inspection No Adverse Event or Action Reported Met with representatives from two plugging contractors to discuss plugging the well. Dug arround wellhead and exposed casinghead for 7" casing about a foot below ground surface.
2481805 Primary Facility 2016-04-05 Routine/Complete Inspection No Violations Noted THIS ABANDONED WELL AND JACK HAVE NOT BEEN DISTURBED. THE WELL IS SHUT IN BUT GAS IS FLOWING FROM THE STUFFING BOX.
2483584 Primary Facility 2016-05-04 Routine/Partial Inspection No Adverse Event or Action Reported Met w/ third contractor to inspect well and evaluate how well can be plugged.
2509448 Primary Facility 2016-06-16 Routine/Partial Inspection No Adverse Event or Action Reported Visited site to check on gas leak from stuffing box-same as before, minor leak.
2512296 Primary Facility 2016-08-22 Routine/Partial Inspection No Adverse Event or Action Reported Visited site to check staus of well, which appears unchanged. Wellhead still leaking a small amount of gas from the stuffing box.
2529580 Primary Facility 2016-10-17 Routine/Complete Inspection No Viols - Permanently Shut Down Visited site to check status of wellhead. Unchanged from 8/22/16 visit. Well leaking a minor amount of gas from stuffing box.
2547535 Primary Facility 2016-12-28 Routine/Partial Inspection No Violations Noted Visited site to check on well status. No change since last visit on 10/17/16. Well is still leaking small amount of gas from stuffing box.
2678251 Primary Facility 2018-01-04 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site to check well status: unchanged from prior visits. Wellhead leaking a small amount of gas from rod/stuffing box. No fluid leaks detected.
2703953 Primary Facility 2018-03-12 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site prior to tomorrow's pre-bid meeting with plugging contractors at Richland Township Municipal Building. Wellhead remains intact and unchanged from prior inspections.
2704423 Primary Facility 2018-03-12 Routine/Complete Inspection No Violations Noted Inspection in response to an Environmental Good Samaritan Project Proposal for Abandoned Well Plugging received on 2/13/2018. The proposed well plugging operation associated with well 003-22239, PGH Cut Flowers 1, is located near 4137 Bakerstown Road. No observation of accelerated erosion or sedimentation in relation to the well. The well site does not have an access road. No observation of a stream, spring, water body, wetland, or water feature in the immediate vicinity of the proposed operations that would require additional environmental permitting. The Department notes that a pond is located approximately 750’ down gradient from the well. The Department recommends that the Operator develop an E&S plan that outlines the placement and type of temporary BMPs to ensure that earth disturbance activity and related erosion and sedimentation is minimized. The operation of plugging this well will improve and not worsen the current site conditions.
2705414 Primary Facility 2018-03-13 Routine/Partial Inspection No Viols - Permanently Shut Down Visited site as part of pre-bid meeting with representatives of plugging contractors and Richland Township after meeting at the Municipal Building. Discussed site conditions and plugging details.
2736300 Primary Facility 2018-05-23 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging excavating/building site in preparation for rig. Pump jack removed.
2736302 Primary Facility 2018-05-23 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging rigging up on well to begin pulling rods.
2744892 Primary Facility 2018-05-24 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging pulled rods and tubing, shut in well. Tubing was reduced from 2 3/8" to 1 1/2" ~ 1 joint down from surface.
2744902 Primary Facility 2018-05-25 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging attempted to TIH with 2 3/8" work string, but hit obstruction at ~15' and unable to get deeper. Will get load of 1 1/2" tubing to attempt to get to bottom and set bottom plug.
2745358 Primary Facility 2018-05-29 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging making final preparations to site to prepare for plugging. Ready to TIH with 1 1/2" tubing to spot bottom hole plug. Well is being blown down, making steady flow of gas. Gas appears to be dry and is low pressure.
2745416 Primary Facility 2018-05-30 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging waiting on delivery of center spear to pull 3 1/2" casing. Also waiting on wireline truck to tag TOC plug and cut 3 1/2".
2745418 Primary Facility 2018-05-30 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging TIH with center spear after loggers tagged TOC at 1630' and cut 3 1/2" casing collar at 1606' above packer. Casing pulled free, TOOH with casing.
2745434 Primary Facility 2018-05-30 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging was able to retrieve all of the 3 1/2" casing, including packer, as the casing did not part at the cut collar. Loggers ran CBL, found 5" casing backside cemented up to ~1580' (TOC plug at 1630'). Will perf casing to prepare to plug to surface.
2745441 Primary Facility 2018-05-31 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging was pumping cement plug at time of inspection.
2745443 Primary Facility 2018-05-31 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging pumped three cement plugs (calculated) of 600', 600' and 450' to bring cement to surface. Level dropped a few times and was topped off. Cement circulated up 10"/5" annulus on last two plugs.
2745464 Primary Facility 2018-06-04 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging demobilized all equipment from site, graded site.
2746215 Primary Facility 2018-06-06 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging has not yet seeded and mulched the site.
2746325 Primary Facility 2018-06-08 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging has still not seeded and mulched the site. Called Nick's to check on plans.
2746338 Primary Facility 2018-06-11 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Nick's Well Plugging has seeded and mulched site.
2750256 Primary Facility 2018-06-13 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Mulch remains in place after recent heavy rains. No repairs needed.
2754043 Primary Facility 2018-07-06 Plugging(Includes Plugged/Mined Through) In Compliance with Policy Check site again after more heavy rains. Mulch, soil and grass remain with minimal effect. No repairs needed.

For data sources see[5]

References