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37-005-01550

Well Details

Well ID: 37-005-01550
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Sugarcreek Township
Operator Name: SENECA RESOURCES CO LLC
Well Pad ID:
Farm/Lease Name: WILLIAM J. HARMON 5300
License Status: PLUGGED & ABANDONED
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.945494
Longitude: -79.587808

For data sources see[1][2][3]

Well History

Date Event
1914-08-14 Drilling Completion
1986-01-01 OLD WELL
2012-10-06 Drilling Completion
2012-12-27 FULLY PLUGGED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 NATL FUEL GAS SUPPLY CORP 1075.00 362 0.00 0 0.00 0
1992 NATL FUEL GAS SUPPLY CORP 1,365.00 366 0.00 0 0.00 0
1996 SENECA RESOURCES CO LLC 1196 365 0.00 0 0.00 0
1997 SENECA RESOURCES CO LLC 1337 359 0.00 0 0.00 0
1998 SENECA RESOURCES CO LLC 1331 359 0.00 0 0.00 0
1999 SENECA RESOURCES CO LLC 1213 365 0.00 0 0.00 0
2000 SENECA RESOURCES CO LLC 985.00 365 0.00 0 0.00 0
2001 SENECA RESOURCES CO LLC 814 365 0.00 0 0.00 0
2002 SENECA RESOURCES CO LLC 780 365 0.00 0 0.00 0
2003 SENECA RESOURCES CO LLC 410 364 0.00 0 0.00 0
2004 SENECA RESOURCES CO LLC 750 365 0.00 0 0.00 0
2006 SENECA RESOURCES CO LLC 1217.00 365 0.00 0 0.00 0
2007 SENECA RESOURCES CO LLC 1112.00 365 0.00 0 0.00 0
2008 SENECA RESOURCES CO LLC 1218.00 365 0.00 0 0.00 0
2009 SENECA RESOURCES CO LLC 702.00 365 0.00 0 0.00 0
2010 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2011 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2012 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1861953 Primary Facility 2010-02-02 Complaint Inspection No Violations Noted gas odor complaint - scheduled meeting with operator
1861957 Primary Facility 2010-02-03 Complaint Inspection No Violations Noted equipped - small leak ID'd with meter @ casing - operator to investigate as soon as weather permits
1890223 Primary Facility 2010-06-03 Complaint Inspection No Violations Noted on-site meeting with complainant & operator rep - operator considering plugging gas well
1984140 Primary Facility 2011-06-13 Complaint Inspection No Violations Noted Well needs updated proper identification.
2082531 Primary Facility 2012-07-10 Plugging(Includes Plugged/Mined Through) No Violations Noted Operator rep B. Reeseman notified Department of intent to plug well and in process of submitting paperwork. Production line disconnected from well at time of inspection. Well needs updated proper identification. Wellhead consists of 4" x 2" swage.
2788703 Primary Facility 2018-10-15 Routine/Complete Inspection No Violations Noted This well is tagged and in production. The annulus is open. The well head casing and piping look ok.

For data sources see[6]

References