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37-005-02341

Well Details

Well ID: 37-005-02341
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Kittanning Township
Operator Name: EXCO RESOURCES PA LLC
Well Pad ID:
Farm/Lease Name: MCCLUNE 1
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.747786
Longitude: -79.473311

For data sources see[1][2][3]

Well History

Date Event
1937-12-16 Drilling Completion
1998-07-29 Old Well

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1997 SHAWMUT PROD CORP 0.00 0 0.00 0 0.00 0
1998 SHAWMUT PROD CORP 0.00 0 0.00 0 0.00 0
1999 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2000 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2001 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2002 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2003 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2004 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2005 POWER GAS MKT & TRANS INC 83 365 0.00 0 0.00 0
2006 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2007 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2008 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2009 EXCO RESOURCES PA INC 0.00 0 0.00 0 0.00 0
2010 EXCO RESOURCES PA INC 0.00 0 0.00 0 0.00 0
2011 EXCO RESOURCES PA INC 0.00 0 0.00 0 0.00 0
2012 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2013 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2014 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2015 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2016 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2017 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0
2018 EXCO RESOURCES PA LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2494671 Primary Facility 2016-06-16 Plugging(Includes Plugged/Mined Through) Pending Well tagged-shut in-not equipped for production with gas leaking from ground all around well @ 40% gas from 2' away from well head and 2% gas coming from ground from 8' away from well head. Working with operator to ensure proper plugging of this well.
2494689 Primary Facility 2016-06-20 Plugging(Includes Plugged/Mined Through) Pending Met with DEP WQS Greg Higgins to check head space of closest 2 water wells and basement/foundation of home closest to this leaking well for the potential presence of gas. All readings from two 62S Gas scope meters came back at 0 % LEL for any gas.
2496640 Primary Facility 2016-06-22 Plugging(Includes Plugged/Mined Through) Pending Performed dual inspection with Doug Catalano. Set up FLIR camera-imaged and documented gas coming from ground around this well due to casing leak. Working with operator for proper plugging.
2496646 Primary Facility 2016-06-23 Plugging(Includes Plugged/Mined Through) Pending Met with operator-witnessed well being guaged @ 3.5 ounces-opened to atmosphere-vertical vent installed to allow gas leaking into ground through casing to vent up into atmosphere until well is plugged.
2496657 Primary Facility 2016-06-27 Plugging(Includes Plugged/Mined Through) Pending Checked level of gas at ground level which had been 40% gas before well was opened and vented to atmosphere. Readings had now dropped to 2% gas at ground level. Still working with operator to see this well properly plugged.
2510097 Primary Facility 2016-08-09 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig reached attainable bottom @ 2512'-pulled 1st joint to curculate @ 2480'. After attaining good circulation-began cementing in stages up to 1260' @ time of inspection. All equipment looked ok.
2510237 Primary Facility 2016-08-10 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig tagged cement top @ 1240'-perfed 2 shots per 100' from 1200' to 300'-Rig running tubing back down well bore to cement 2-600' plugs to surface @ time of inspection. All equipment looked ok.

For data sources see[6]

References