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37-005-20743

Well Details

Well ID: 37-005-20743
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Burrell Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: J G KIRKLAND 39
License Status: ACTIVE
Spud Date:
Permit Date: 1964-12-02
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.641156
Longitude: -79.431546

For data sources see[1][2][3]

Well History

Date Event
1893-01-01 Drilling Completion
1893-12-30 OLD WELL
1964-12-02 New Permit Application
1965-02-18 Drilling Completion
1966-01-01 DRILLED DEEPER

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 2159.00 334 0.00 0 0.00 0
1996 906 365 0.00 0 0.00 0
1998 1137 313 0.00 0 0.00 0
1999 CONSOL GAS CO 2198 365 0.00 0 0.00 0
2000 CONSOL GAS CO 1014 365 0.00 0 0.00 0
2001 CONSOL GAS CO 775 365 0.00 0 0.00 0
2002 CONSOL GAS CO 1119 365 0.00 0 0.00 0
2003 CONSOL GAS CO 1302 365 0.00 0 0.00 0
2005 CONSOL GAS CO 1068 365 0.00 0 0.00 0
2006 CONSOL GAS CO 717.00 365 0.00 0 0.00 0
2007 CONSOL GAS CO 463.00 365 0.00 0 0.00 0
2008 CONSOL GAS CO 850.00 365 0.00 0 0.00 0
2009 CONSOL GAS CO 925.00 365 0.00 0 0.00 0
2010 CONSOL GAS CO 796.00 365 0.00 0 0.00 0
2011 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2012 CNX GAS CO LLC 832.00 366 0.00 0 0.00 0
2013 CNX GAS CO LLC 732.00 365 0.00 0 0.00 0
2014 CNX GAS CO LLC 691.00 365 0.00 0 0.00 0
2015 CNX GAS CO LLC 546.00 365 0.00 0 0.00 0
2016 CNX GAS CO LLC 469.00 366 0.00 0 0.00 0
2017 CNX GAS CO LLC 445.00 365 0.00 0 0.00 0
2018 CNX GAS CO LLC 556.00 365 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 496.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2006 CONSOL GAS CO Brine 0.00 Bbl Other

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2246256 Primary Facility 2014-02-19 Administrative/File Review In Compliance with Policy Admin inspt. At 1513, Operator representative Jamie Komonich notified Department via phone of water leaking out of wellhead of conventional well. Well-tender notified Operator on 2/10/2014 of orange discoloration of wellhead and surrounding soils. Water ponding around wellhead.
2247732 Primary Facility 2014-02-20 Routine/Complete Inspection No Violations Noted Site inspected at the request of the operator after the operator observed what appeared to be contaminated fluids emerging in the vicinity of the well head. Well was equipped for production. A discharge of what appeared to be mine and/or coal influenced water was emerging near the well-head. It did not appear that the contaminated water was orginating from or related to the well.
2253928 Primary Facility 2014-03-04 Routine/Complete Inspection Pending Anticipating on sampling weather permitting; Inspection result pending on sample analysis

For data sources see[7]

References