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Well ID: 37-005-20743 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Armstrong | |
Municipality: Burrell Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: J G KIRKLAND 39 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 1964-12-02 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.641156 | |
Longitude: -79.431546 |
Date | Event |
---|---|
1893-01-01 | Drilling Completion |
1893-12-30 | OLD WELL |
1964-12-02 | New Permit Application |
1965-02-18 | Drilling Completion |
1966-01-01 | DRILLED DEEPER |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | 2159.00 | 334 | 0.00 | 0 | 0.00 | 0 | |
1996 | 906 | 365 | 0.00 | 0 | 0.00 | 0 | |
1998 | 1137 | 313 | 0.00 | 0 | 0.00 | 0 | |
1999 | CONSOL GAS CO | 2198 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | CONSOL GAS CO | 1014 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | CONSOL GAS CO | 775 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | CONSOL GAS CO | 1119 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | CONSOL GAS CO | 1302 | 365 | 0.00 | 0 | 0.00 | 0 |
2005 | CONSOL GAS CO | 1068 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | CONSOL GAS CO | 717.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | CONSOL GAS CO | 463.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | CONSOL GAS CO | 850.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | CONSOL GAS CO | 925.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | CONSOL GAS CO | 796.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CNX GAS CO LLC | 832.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | CNX GAS CO LLC | 732.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | CNX GAS CO LLC | 691.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | CNX GAS CO LLC | 546.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | CNX GAS CO LLC | 469.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | CNX GAS CO LLC | 445.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | CNX GAS CO LLC | 556.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | ALLIANCE PETRO CO LLC | 496.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2006 | CONSOL GAS CO | Brine | 0.00 Bbl | Other |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2246256 | Primary Facility | 2014-02-19 | Administrative/File Review | In Compliance with Policy | Admin inspt. At 1513, Operator representative Jamie Komonich notified Department via phone of water leaking out of wellhead of conventional well. Well-tender notified Operator on 2/10/2014 of orange discoloration of wellhead and surrounding soils. Water ponding around wellhead. |
2247732 | Primary Facility | 2014-02-20 | Routine/Complete Inspection | No Violations Noted | Site inspected at the request of the operator after the operator observed what appeared to be contaminated fluids emerging in the vicinity of the well head. Well was equipped for production. A discharge of what appeared to be mine and/or coal influenced water was emerging near the well-head. It did not appear that the contaminated water was orginating from or related to the well. |
2253928 | Primary Facility | 2014-03-04 | Routine/Complete Inspection | Pending | Anticipating on sampling weather permitting; Inspection result pending on sample analysis |
For data sources see[7]