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37-005-27485

Well Details

Well ID: 37-005-27485
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Cowanshannock Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: J M THOMPSON 3
License Status: ACTIVE
Spud Date:
Permit Date: 2004-02-10
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.819209
Longitude: -79.225044

For data sources see[1][2][3]

Well History

Date Event
2004-02-10 New Permit Application
2004-06-04 Performed Spud Operation
2004-06-07 Drilling Completion
2004-06-17 Perforation
2004-08-18 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2004 PHILLIPS EXPLORATION INC 11645 121 0.00 0 0.00 0
2005 PHILLIPS EXPLORATION INC 29514 365 0.00 0 0.00 0
2006 PHILLIPS EXPLORATION INC 19086.00 282 0.00 0 0.00 0
2007 PHILLIPS EXPLORATION INC 17545.00 365 0.00 0 0.00 0
2008 PHILLIPS EXPLORATION INC 13738.00 335 0.00 0 0.00 0
2009 PHILLIPS EXPLORATION INC 11098.00 365 0.00 0 0.00 0
2010 PHILLIPS EXPLORATION INC 9,608.00 365 0.00 0 0.00 0
2011 PHILLIPS EXPLORATION INC 8,317.00 363 0.00 0 0.00 0
2012 XTO ENERGY INC 7,740.00 366 0.00 0 0.00 0
2013 XTO ENERGY INC 6,614.00 365 0.00 0 0.00 0
2014 XTO ENERGY INC 5,846.00 361 0.00 0 0.00 0
2015 XTO ENERGY INC 6,061.00 365 0.00 0 0.00 0
2016 XTO ENERGY INC 5,586.90 366 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 4,394.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 4,893.00 365 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 5,402.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2016 XTO ENERGY INC Produced Fluid 20 Bbl CENT WASTE TRT FAC NPDES PA0095273
2016 XTO ENERGY INC Produced Fluid 20.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1343970 Primary Facility 2004-06-09 Drilling/Alteration No Violations Noted LK Rig 6 completed drilling well and moved off. ES and Pit ok.
2462341 Primary Facility 2016-03-07 Routine/Complete Inspection No Violations Noted Well tagged-in production. Annulus is shut. Well head casing-equipment and 100 bbl tank look ok.

For data sources see[7]

References