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Well ID: 37-019-01455 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Butler | |
Municipality: Clinton Township | |
Operator Name: HERMAN RIEMER GAS CO | |
Well Pad ID: | |
Farm/Lease Name: BREWER | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.714806 | |
Longitude: -79.833889 |
Date | Event |
---|---|
1905-01-01 | Drilling Completion |
1995-08-02 | OLD WELL |
2019-01-03 | Begin Plugging |
2019-02-27 | Finished Plugging |
2020-01-30 | Fully Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2005 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2018 | HERMAN RIEMER GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2597710 | Primary Facility | 2017-05-23 | Routine/Partial Inspection | No Violations Noted | |
2825026 | Primary Facility | 2019-01-09 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | NOI received on 1/4/19 with plugging scheduled to begin on 1/8/19. Inspection shows rig over the well bore with tubulars tripped out. Operations currently shut down. Spoke to the rig operator by phone and they are currently waiting on lines (one call) to be marked to be able to dig a pit. Bond log has already been run. Bottom plugs are scheduled to be set on 1/14/19. |
2827688 | Primary Facility | 2019-01-16 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Previous inspection showed NOI received on 1/4/19 with plugging scheduled to begin on 1/8/19. Previously rig was waiting on lines (one call) to be marked to be able to dig a pit. Inspection shows lines have been marked with pit liner and excavator on site. Operations currently shit down. |
2843633 | Primary Facility | 2019-02-05 | Routine/Partial Inspection | No Violations Noted | Due to weather conditions met plugging contractor (Toby Dishong) in Saxonburg to discuss plugging procedures. Following information gathered from Toby. Well records limited, Td 2813'. 6-1/4 593' producing horizon 2728'. Logs ran and determined 3" down to 2750' and showed free pipe from 2750' to 1850' and bond from 1850' to 1630'. Three inch perf every 100' from 2650' to 1950' and then at 1650' & 1550'. Three inch was then shot off at 1400' and then the remaining 3" was tripped out. Well bore cemented from 2750' to 1435'. Old record shows 4-7/8 to 1480'. Log was able to determine 4-7/8 down to 1375'. Rig was unable to pull the 4-7/8. 4-7/8 was perf at 1300' 1200' 1100' then cut at 1000' Pipe still hung and was shot again at 800'. Currently anticipating cementing from 1435' to 800'. Rig will then attempted to pull 4-7/8 from 800'. |
For data sources see[6]