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37-019-01455

Well Details

Well ID: 37-019-01455
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Country: United States
State: Pennsylvania
County: Butler
Municipality: Clinton Township
Operator Name: HERMAN RIEMER GAS CO
Well Pad ID:
Farm/Lease Name: BREWER
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.714806
Longitude: -79.833889

For data sources see[1][2][3]

Well History

Date Event
1905-01-01 Drilling Completion
1995-08-02 OLD WELL
2019-01-03 Begin Plugging
2019-02-27 Finished Plugging
2020-01-30 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2007 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2009 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2010 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2011 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2012 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2013 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2014 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2015 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2016 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2017 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0
2018 HERMAN RIEMER GAS CO 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2597710 Primary Facility 2017-05-23 Routine/Partial Inspection No Violations Noted
2825026 Primary Facility 2019-01-09 Plugging(Includes Plugged/Mined Through) No Violations Noted NOI received on 1/4/19 with plugging scheduled to begin on 1/8/19. Inspection shows rig over the well bore with tubulars tripped out. Operations currently shut down. Spoke to the rig operator by phone and they are currently waiting on lines (one call) to be marked to be able to dig a pit. Bond log has already been run. Bottom plugs are scheduled to be set on 1/14/19.
2827688 Primary Facility 2019-01-16 Plugging(Includes Plugged/Mined Through) No Violations Noted Previous inspection showed NOI received on 1/4/19 with plugging scheduled to begin on 1/8/19. Previously rig was waiting on lines (one call) to be marked to be able to dig a pit. Inspection shows lines have been marked with pit liner and excavator on site. Operations currently shit down.
2843633 Primary Facility 2019-02-05 Routine/Partial Inspection No Violations Noted Due to weather conditions met plugging contractor (Toby Dishong) in Saxonburg to discuss plugging procedures. Following information gathered from Toby. Well records limited, Td 2813'. 6-1/4 593' producing horizon 2728'. Logs ran and determined 3" down to 2750' and showed free pipe from 2750' to 1850' and bond from 1850' to 1630'. Three inch perf every 100' from 2650' to 1950' and then at 1650' & 1550'. Three inch was then shot off at 1400' and then the remaining 3" was tripped out. Well bore cemented from 2750' to 1435'. Old record shows 4-7/8 to 1480'. Log was able to determine 4-7/8 down to 1375'. Rig was unable to pull the 4-7/8. 4-7/8 was perf at 1300' 1200' 1100' then cut at 1000' Pipe still hung and was shot again at 800'. Currently anticipating cementing from 1435' to 800'. Rig will then attempted to pull 4-7/8 from 800'.

For data sources see[6]

References