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37-033-23168

Well Details

Well ID: 37-033-23168
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Country: United States
State: Pennsylvania
County: Clearfield
Municipality: Bell Township
Operator Name: FAIRMAN CORP
Well Pad ID:
Farm/Lease Name: POWELL
License Status: Plugged and Abandoned
Spud Date: 1989-05-23
Permit Date: 1989-04-19
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.886484
Longitude: -78.736174

For data sources see[1][2][3]

Well History

Date Event
1989-04-19 New Permit Application
1989-05-02 Perforation
1989-05-03 Perforation
1989-05-03 Performed Stimulation
1989-05-23 Performed Spud Operation
1989-05-26 Drilling Completion
1989-07-31 Fully Plugged

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1989-05-03 SAND 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 FAIRMAN OIL & GAS CO INC 13490.00 365 0.00 0 0.00 0
1992 FAIRMAN DRILLING CO 19861.00 365 0.00 0 0.00 0
1993 FAIRMAN DRILLING CO 16679.00 365 0.00 0 0.00 0
1994 FAIRMAN DRILLING CO 14511.00 365 0.00 0 0.00 0
1996 FAIRMAN DRILLING CO 7822 365 0.00 0 0.00 0
1997 FAIRMAN DRILLING CO 7219 365 0.00 0 0.00 0
1998 FAIRMAN DRILLING CO 5111 365 0.00 0 0.00 0
1999 FAIRMAN DRILLING CO 6029 365 0.00 0 0.00 0
2000 FAIRMAN DRILLING CO 5055 365 0.00 0 0.00 0
2001 FAIRMAN DRILLING CO 4408 365 0.00 0 0.00 0
2002 FAIRMAN DRILLING CO 4172 365 0.00 0 0.00 0
2003 FAIRMAN CORP 1352 365 0.00 0 0.00 0
2010 FAIRMAN CORP 2,488.00 365 0.00 0 0.00 0
2011 FAIRMAN CORP 2,333.70 365 0.00 0 0.00 0
2012 FAIRMAN CORP 2,248.88 365 0.00 0 0.00 0
2013 FAIRMAN CORP 2,157.90 365 0.00 0 0.00 0
2014 FAIRMAN CORP 1,816.40 334 0.00 0 0.00 0
2015 FAIRMAN CORP 658.6 120 0.00 0 0.00 0
2016 FAIRMAN CORP 0.00 0 0.00 0 0.00 0
2017 FAIRMAN CORP 239.00 120 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1991 FAIRMAN OIL & GAS CO INC Brine 40.00 Bbl
1994 FAIRMAN DRILLING CO Brine 60.00 Bbl
1996 FAIRMAN DRILLING CO Brine 75.00 Bbl Brine or Industrial Waste Treatment Plt PA0026310
1997 FAIRMAN DRILLING CO Brine 10.00 Bbl Brine or Industrial Waste Treatment Plt PA0026310
1998 FAIRMAN DRILLING CO Brine 10.00 Bbl Brine or Industrial Waste Treatment Plt 0026310
2002 FAIRMAN DRILLING CO Brine 0.00 Bbl Brine or Industrial Waste Treatment Plt PA0026310
2017 FAIRMAN CORP Produced Fluid 37.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0028428

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2592104 Primary Facility 2017-05-10 Routine/Complete Inspection No Violations Noted Per electronic notification contractor began plugging operations on the Fairman Drilling, Powell #12 (033-23168) conventional well on 5/9/2017. PADEP plugging inspector on location as well. Small plastic lined earthen pit dug immediately adjacent to the workover rig. Rig set up on well, and tripping out with rig pipe and stacking on trailer during this inspection. Silt fence incised in the existing sod along the east edge of the location, with spoil from pit excavation adjacent. Site is essentially flat with no surface water in the vicinity.
2592978 Primary Facility 2017-05-11 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspection of Fairman’s Powell # 12 well conducted May 10, 2017 at approximately 10:00 am. Rig is on location for plugging operations. Allegheny Cementers are on location. Attainable bottom tagged reportedly at 3100’. Allegheny pumped cement plug from bottom, calculated volume back to cement top behind 4 ½” (1475’ from cement top log). The rig pulled up out of plug and washed off. They’ll WOC overnight, wireline will run in tomorrow to shoot off 4 1/2” @ 1475’ and finish the P&A with Allegheny pumping another plug from the 4 ½” csg stub back to ~1239’ (50’ inside 8 5/8”). No issues.
2596684 Primary Facility 2017-05-22 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspection of Fairman’s Powell # 12 well conducted May 22, 2017 at approximately 10:56 am. The Plugging Rig is off location following plugging operations. Vent pipe installed atop casing. No gas was detected at the vent using an Altair 5x gas meter.
2601702 Primary Facility 2017-06-07 Administrative/File Review No Violations Noted June 7, 2017, Fairman's Powell #12 (033-23168) Plugging Certificate received, reviewed, signed and sent to file. No issues
2775129 Primary Facility 2018-09-11 Site Restoration No Violations Noted Restoration inspection on September 11, 2018 with Santo Adams of Fairman Corporation at restored conventional well 033-23168. The well has been plugged and the area surrounding the plugged well has been restored. The restored site is very well vegetated.

Per this inspection I approve the well site restoration report submitted for 033-23168.

354822 Primary Facility 1989-04-27 Routine/Complete Inspection No Violations Noted STAKED
354823 Primary Facility 1989-05-05 Routine/Complete Inspection No Violations Noted STAKED
354824 Primary Facility 1989-05-23 Drilling/Alteration No Violations Noted AT 30'
354825 Primary Facility 1989-05-26 Routine/Complete Inspection No Violations Noted TD AT 4342'
354826 Primary Facility 1989-06-01 Routine/Complete Inspection No Violations Noted E&S, PITS OK
364900 Primary Facility 1990-03-01 Site Restoration No Violations Noted SITE RESTORED; NO TANK

For data sources see[8]

References