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37-033-23184

Well Details

Well ID: 37-033-23184
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Country: United States
State: Pennsylvania
County: Clearfield
Municipality: Bell Township
Operator Name: FAIRMAN CORP
Well Pad ID:
Farm/Lease Name: POWELL
License Status: Plugged and Abandoned
Spud Date: 1989-10-24
Permit Date: 1989-08-03
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.896434
Longitude: -78.734460

For data sources see[1][2][3]

Well History

Date Event
1989-08-03 New Permit Application
1989-10-24 Performed Spud Operation
1989-10-26 Drilling Completion
1989-11-07 Perforation
1989-11-07 Performed Stimulation
1989-12-29 Fully Plugged

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1989-11-07 SAND 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 FAIRMAN OIL & GAS CO INC 13488.00 365 0.00 0 0.00 0
1992 FAIRMAN DRILLING CO 19860.00 365 0.00 0 0.00 0
1993 FAIRMAN DRILLING CO 16677.00 365 0.00 0 0.00 0
1994 FAIRMAN DRILLING CO 14509.00 365 0.00 0 0.00 0
1996 FAIRMAN DRILLING CO 7825 365 0.00 0 0.00 0
1997 FAIRMAN DRILLING CO 7215 365 0.00 0 0.00 0
1998 FAIRMAN DRILLING CO 5108 365 0.00 0 0.00 0
1999 FAIRMAN DRILLING CO 6024 365 0.00 0 0.00 0
2000 FAIRMAN DRILLING CO 5045 365 0.00 0 0.00 0
2001 FAIRMAN DRILLING CO 4407 365 0.00 0 0.00 0
2002 FAIRMAN DRILLING CO 4168 365 0.00 0 0.00 0
2003 FAIRMAN CORP 1352 365 0.00 0 0.00 0
2010 FAIRMAN CORP 2,488.00 365 0.00 0 0.00 0
2011 FAIRMAN CORP 2,333.70 365 0.00 0 0.00 0
2012 FAIRMAN CORP 2,248.88 365 0.00 0 0.00 0
2013 FAIRMAN CORP 2,157.90 365 0.00 0 0.00 0
2014 FAIRMAN CORP 1,816.40 334 0.00 0 0.00 0
2015 FAIRMAN CORP 658.6 120 0.00 0 0.00 0
2016 FAIRMAN CORP 0.00 0 0.00 0 0.00 0
2017 FAIRMAN CORP 214.00 150 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1991 FAIRMAN OIL & GAS CO INC Brine 130.00 Bbl
1994 FAIRMAN DRILLING CO Brine 50.00 Bbl
1996 FAIRMAN DRILLING CO Brine 10.00 Bbl Brine or Industrial Waste Treatment Plt PA0026310
1997 FAIRMAN DRILLING CO Brine 10.00 Bbl Brine or Industrial Waste Treatment Plt PA0026310
1998 FAIRMAN DRILLING CO Brine 10.00 Bbl Brine or Industrial Waste Treatment Plt 0026310
2002 FAIRMAN DRILLING CO Brine 0.00 Bbl Brine or Industrial Waste Treatment Plt PA0026310
2017 FAIRMAN CORP Produced Fluid 8.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0028428

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2590925 Primary Facility 2017-05-04 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspection of Fairman’s Powell # 15 well conducted May 4, 2017 at about 10:30 am. A plugging rig is on location for plugging operations. They tagged attainable bottom approximately 30’ below bottom perfs. Allegheny cementers pumped the bottom cement plug in the production casing from attainable bottom to ~1400’ (freepoint) where wireline will attempt to shoot-off pipe, the rig will pull production casing, and cementers will pump last plug to 50’ inside the surface casing to complete the P&A. No issues.
2592103 Primary Facility 2017-05-10 Routine/Complete Inspection No Violations Noted Plugging operations at the Powell #15 well begun on 5/3/2017, and now completed. PADEP and contractor checked for presence of gas at the open 8 5/8" casing collar at surface, no bubbles and no detectable gas. Small lined pit used for cement returns during plugging has been backfilled, and the entire site has been restored to approximate original contour. Well monument/vent line is being fabricated at the shop and will be threaded into the casing collar. Existing meter run with line pressure and pressure differential remains in use. Powell #15 line connection to the line drip has been removed and drip inlet shut with a threaded plug. Site ready for re-seeding and final restoration and that work is expected to be completed this week.
2592983 Primary Facility 2017-05-10 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspection of Fairman’s Powell # 15 well conducted May 10, 2017 at approximately 11 am following plugging operations. The rig is off location, the 8 5/8” casing collar extends above ground level, full of gravel from the shoe isolation plug and standing water on top. There was no active bubbling observed and no gas detected with an Altair 5x gas meter. The operator will soon place marker on the casing. No issues.
2601709 Primary Facility 2017-06-07 Administrative/File Review No Violations Noted June 7, 2017, Fairman's Powell #15 (033-23184) Plugging Certificate received, reviewed, signed and sent to file. No issues
2785287 Primary Facility 2018-10-05 Site Restoration No Violations Noted Fairman Corporation has submitted a well site restoration report for plugged well 033-23184 to the Department. On October 5, 2018 Department representative Sue Herzing conducted a well site restoration inspection at the above listed plugged well site. The plugged well is represented with a monument containing the well permit number. The area surrounding the plugged well has been restored and is well vegetated.

Per this inspection, the Department is approving the well site restoration report for plugged well 033-23184.

354880 Primary Facility 1989-10-23 Drilling/Alteration No Violations Noted RIGGING UP
354881 Primary Facility 1989-10-23 Routine/Complete Inspection No Violations Noted E&S, PITS OK
354882 Primary Facility 1989-10-27 Routine/Complete Inspection No Violations Noted DRILLED TO 3480'
354883 Primary Facility 1989-11-01 Routine/Complete Inspection No Violations Noted E&S, PITS OK
366136 Primary Facility 1990-07-23 Site Restoration No Violations Noted SITE RESTORED

For data sources see[8]

References