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Well ID: 37-047-23737 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Elk | |
Municipality: Ridgway Township | |
Operator Name: DIVERSIFIED OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: FEE HEARTWOOD FOREST LANDS 38056 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 2006-02-10 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.499562 | |
Longitude: -78.643150 |
Date | Event |
---|---|
2006-02-10 | New Permit Application |
2006-05-17 | Drilling Completion |
2006-06-16 | Performed Spud Operation |
2006-08-04 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2007 | SENECA RESOURCES CO LLC | 3478.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | SENECA RESOURCES CO LLC | 2815.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | SENECA RESOURCES CO LLC | 1907.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | SENECA RESOURCES CO LLC | 1,162.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | SENECA RESOURCES CO LLC | 2,090.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | SENECA RESOURCES CO LLC | 2,366.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2013 | SENECA RESOURCES CO LLC | 1,209.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | SENECA RESOURCES CO LLC | 1,315.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | SENECA RESOURCES CO LLC | 1,089.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | DIVERSIFIED OIL & GAS LLC | 967.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | DIVERSIFIED OIL & GAS LLC | 940.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | DIVERSIFIED OIL & GAS LLC | 1,450.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | DIVERSIFIED OIL & GAS LLC | 963.00 | 334 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2012 | SENECA RESOURCES CO LLC | Produced Fluid | 35.00 Bbl | INJECTION DISPOSAL WELL | 34-007-24355 |
2013 | SENECA RESOURCES CO LLC | Produced Fluid | 35.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NW005 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2682411 | Primary Facility | 2018-01-12 | Routine/Complete Inspection | No Violations Noted | On 1/12/18 at 1100 hrs. i conducted a routine inspection of Diversified's 38056 well site (API 047-23737) in Ridgway, Elk Co. The well is equipped for production and a well tag and site ID sign are present. The well pad is permanently stabilized. There are no violations noted for this inspection. |
2682782 | Primary Facility | 2018-01-16 | Routine/Complete Inspection | No Violations Noted | This well was reported to me as possibly leaking. The well is currently shut in and not producing. Production was reported for 2016. I could smell gas as I entered the location and was able to detect 6% methane coming from a 2" vent that is open on the 7" casing. No gas was detected leaking anywhere else. No bubbles or gas was detected on the back side of the conductor or casing. |
For data sources see[7]