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37-047-23737

Well Details

Well ID: 37-047-23737
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Country: United States
State: Pennsylvania
County: Elk
Municipality: Ridgway Township
Operator Name: DIVERSIFIED OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: FEE HEARTWOOD FOREST LANDS 38056
License Status: ACTIVE
Spud Date:
Permit Date: 2006-02-10
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.499562
Longitude: -78.643150

For data sources see[1][2][3]

Well History

Date Event
2006-02-10 New Permit Application
2006-05-17 Drilling Completion
2006-06-16 Performed Spud Operation
2006-08-04 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2007 SENECA RESOURCES CO LLC 3478.00 365 0.00 0 0.00 0
2008 SENECA RESOURCES CO LLC 2815.00 365 0.00 0 0.00 0
2009 SENECA RESOURCES CO LLC 1907.00 365 0.00 0 0.00 0
2010 SENECA RESOURCES CO LLC 1,162.00 365 0.00 0 0.00 0
2011 SENECA RESOURCES CO LLC 2,090.00 365 0.00 0 0.00 0
2012 SENECA RESOURCES CO LLC 2,366.00 365 0.00 0 0.00 0
2013 SENECA RESOURCES CO LLC 1,209.00 365 0.00 0 0.00 0
2014 SENECA RESOURCES CO LLC 1,315.00 365 0.00 0 0.00 0
2015 SENECA RESOURCES CO LLC 1,089.00 365 0.00 0 0.00 0
2016 DIVERSIFIED OIL & GAS LLC 967.00 365 0.00 0 0.00 0
2017 DIVERSIFIED OIL & GAS LLC 940.00 365 0.00 0 0.00 0
2018 DIVERSIFIED OIL & GAS LLC 1,450.00 365 0.00 0 0.00 0
2019 DIVERSIFIED OIL & GAS LLC 963.00 334 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2012 SENECA RESOURCES CO LLC Produced Fluid 35.00 Bbl INJECTION DISPOSAL WELL 34-007-24355
2013 SENECA RESOURCES CO LLC Produced Fluid 35.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NW005

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2682411 Primary Facility 2018-01-12 Routine/Complete Inspection No Violations Noted On 1/12/18 at 1100 hrs. i conducted a routine inspection of Diversified's 38056 well site (API 047-23737) in Ridgway, Elk Co. The well is equipped for production and a well tag and site ID sign are present. The well pad is permanently stabilized. There are no violations noted for this inspection.
2682782 Primary Facility 2018-01-16 Routine/Complete Inspection No Violations Noted This well was reported to me as possibly leaking. The well is currently shut in and not producing. Production was reported for 2016. I could smell gas as I entered the location and was able to detect 6% methane coming from a 2" vent that is open on the 7" casing. No gas was detected leaking anywhere else. No bubbles or gas was detected on the back side of the conductor or casing.

For data sources see[7]

References