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37-063-00346

Well Details

Well ID: 37-063-00346
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Rayne Township
Operator Name: PEOPLES TWP LLC
Well Pad ID:
Farm/Lease Name: B WYNCOOP 114A 1
License Status: PLUGGED & ABANDONED
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.747336
Longitude: -79.067565

For data sources see[1][2][3]

Well History

Date Event
1925-11-14 Drilling Completion
1942-05-09 Drilling Completion
1986-04-14 DRILLED DEEPER
1986-04-14 OLD WELL
2004-11-05 Drilling Completion
2010-02-25 FULLY PLUGGED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 PEOPLES TWP LLC 234.00 365 0.00 0 0.00 0
1992 PEOPLES TWP LLC 176.00 366 0.00 0 0.00 0
1993 PEOPLES TWP LLC 234.00 365 0.00 0 0.00 0
1994 PEOPLES TWP LLC 83.00 250 0.00 0 0.00 0
1995 PEOPLES TWP LLC 124.00 365 0.00 0 0.00 0
1996 PEOPLES TWP LLC 85 365 0.00 0 0.00 0
1997 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
1998 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
1999 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
2000 PEOPLES TWP LLC 1 366 0.00 0 0.00 0
2001 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
2002 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
2003 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0
2004 PEOPLES TWP LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1387245 Primary Facility 2004-10-19 Plugging(Includes Plugged/Mined Through) No Violations Noted Key Well cleaned out to 3378' Steel cellar and E&S OK.
1387270 Primary Facility 2004-10-20 Plugging(Includes Plugged/Mined Through) No Violations Noted Key Well removed ~270' of 3 1/2 production string. Waiting on casing spear from Baker Services. E&S OK. First plug set from 3378' to ~3103'.
1394936 Primary Facility 2004-10-27 Plugging(Includes Plugged/Mined Through) No Violations Noted Key energy Tripping out Fish (2735' of 3 1/2'). Pit and E&S Ok.
1394937 Primary Facility 2004-10-29 Plugging(Includes Plugged/Mined Through) No Violations Noted Key Well Service preparing to clean out caved well bore w/ fluid. Pit and E&S OK.

For data sources see[6]

References