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Well ID: 37-065-23619 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Jefferson | |
Municipality: McCalmont Township | |
Operator Name: DANNIC ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: ALGIROD & JULIAN PARIS 1 | |
License Status: ACTIVE | |
Spud Date: 1992-12-03 | |
Permit Date: 1992-11-13 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.017670 | |
Longitude: -78.962830 |
Date | Event |
---|---|
1992-11-13 | New Permit Application |
1992-12-03 | Performed Spud Operation |
1992-12-07 | Drilling Completion |
1993-01-01 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1994 | 1052.00 | 365 | 0.00 | 0 | 0.00 | 0 | |
2004 | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 | |
2014 | WILLIAM L HORNER ENERGY | 30.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | DANNIC ENERGY CORP | 126.84 | 153 | 0.00 | 0 | 0.00 | 0 |
2016 | DANNIC ENERGY CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | DANNIC ENERGY CORP | 49.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | DANNIC ENERGY CORP | 219.72 | 121 | 0.00 | 0 | 0.00 | 0 |
2019 | DANNIC ENERGY CORP | 160.99 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
1994 | Brine | 221.00 Bbl | |||
2018 | DANNIC ENERGY CORP | Produced Fluid | 80.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0028428 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2761851 | Primary Facility | 2018-08-08 | Routine/Complete Inspection | No Violations Noted | This well was drilled in an abandoned agricultural area off of Team Road in December 1992. No violations were noted during this inspection, but several places of plastic pipe and a section of steel line have been left on site that must be removed, and the brine tank drain valve and blow line must be replaced. The Paris well sites will be inspected again in approximately two weeks. Violations will be issued at that time unless the referenced issues have been corrected. |
2769165 | Primary Facility | 2018-08-28 | Routine/Partial Inspection | No Violations Noted | At the time of inspection, well was producing. The valve for tubing was closed, but it appeared production was coming from the casing. Those valves were open. There were 2 separators hooked up, with one having a gauge reading 20 psi. There was also a drip catch installed. A chart was in a meter house that was changed on 7/31. A 100 bbl tank was storing fluids. There was also a house meter hooked up. Production was reported in 2017 as 49 mcf for 365 days. |
2774879 | Primary Facility | 2018-09-14 | Routine/Complete Inspection | Violation(s) Noted | This well was drilled in an abandoned agricultural area off of Team Road in December 1992. During the previous inspection on 8/8/2018 (Inspection Record # 2761851), it was noted that issues were found with material that had been left on site and potential leaks from the brine tank and blow line. At that time it was stated that a follow up inspection would be conducted to ensure that these issues had been corrected. At the time of this inspection, no work on correcting these issues has been completed, and violations have been noted. |
2783107 | Primary Facility | 2018-10-02 | Compliance Evaluation | No Violations Noted | This well was drilled in an abandoned agricultural area off of Team Road in December 1992. During the previous inspection on 9/14/2018 (Inspection Record # 2774879), violations were issued regarding material that had been left on site and potential leaks from the brine tank and blow line. A response to the NOV was received by the Department on 10/1/2018 stating that the material not necessary for production had been removed and that the drain valve and blow line on the brine tank had been replaced. At the time of this inspection, work has been done to correct these issues, and the violations have been closed. |
562999 | Primary Facility | 1993-03-03 | Drilling/Alteration | No Violations Noted |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2774879 | 828013 | 2018-09-14 | 2018-10-02 | OGA3216(C) | Environmental Health & Safety | |
2774879 | 828014 | 2018-09-14 | 2018-10-02 | CSL 402(b) | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
828013 | 369731 | NOV - Notice of Violation | 2018-10-02 | ||||
828014 | 369731 | NOV - Notice of Violation | 2018-10-02 |
For data sources see[7]