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37-111-20236

Well Details

Well ID: 37-111-20236
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Country: United States
State: Pennsylvania
County: Somerset
Municipality: Somerset Township
Operator Name:
Well Pad ID:
Farm/Lease Name: BYERS 1
License Status: ACTIVE
Spud Date:
Permit Date: 2001-05-11
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.066875
Longitude: -79.033977

For data sources see[1][2][3]

Well History

Date Event
2001-05-11 New Permit Application
2001-05-23 Performed Spud Operation
2001-06-01 Drilling Completion
2002-04-29 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2006 MID EAST OIL CO 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1793866 Primary Facility 2009-04-17 Drilling/Alteration Violation(s) Noted Based on records, well was completed on 6/1/01 to a depth of 5,640 ft. from grade. On 3/22/02, WRAC submitted and approved by the DEP. During the inspection, well was located on hillside of agicultural field along Apple Arches Road. The well shows an outside flush 13" conductor pipe with an inside 7" pipe. The annulus between the pipes appears grouted. A wire screen was welded inside the 7" inch pipe. No well tag present on the well. Based on records, a plug report could not be located at the DEP. The site has not been restored. Mounds of unconsolidated material remain at the site.
1819792 Primary Facility 2009-08-04 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Meeting held with Mid East Oil (Lance Cassidy) and DEP (Ed Renwick, Paul Wyrwas, Chad Eisenman and April Wieland) to review 4/17/09 inspection. According to Mid East, well was drilled to TD depth but was never stimulated and was not properly abandoned. Pits were restored and mound of soil was remaining top soil which is protecting the well from agricultural activity. DEP requested that Mid East install a vent pipe over the well to prevent material from entering the well. As indicated in the DEP meeting, Mid East is in the process of abandoning this well according to Oil and Gas regulations. No new violation recorded since the 4/17/09 inspection. However, these violations have not been corrected by Mid East Oil.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1793866 561649 04/17/2009 2009-04-17 210UNPLUG - Failure to plug a well upon abandonment Administrative
1793866 561650 04/17/2009 2009-04-17 201TAG - Failure to install, in a permanent manner, the permit number on a completed well Administrative
1793866 561651 04/17/2009 2009-04-17 102.4 - Failure to minimize accelerated erosion, implement E&S plan, maintain E&S controls. Failure to stabilize site until total site restoration under OGA Sec 206(c)(d) Environmental Health & Safety
1793866 561652 04/17/2009 2009-04-17 206REST - Failure to restore site w/in 9 months of completion of drilling or plugging Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
561649 245446 NOV - Notice of Violation Unresolvable 2011-01-04
561650 245446 NOV - Notice of Violation Unresolvable 2011-01-04
561651 245446 NOV - Notice of Violation Unresolvable 2011-01-04
561652 245446 NOV - Notice of Violation Unresolvable 2011-01-04

For data sources see[6]

References