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Well ID: 37-115-20468 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Susquehanna | |
Municipality: Forest Lake Township | |
Operator Name: BKV OPR LLC | |
Well Pad ID: 145322 | |
Farm/Lease Name: BAKER 4H | |
License Status: | |
Spud Date: | |
Permit Date: 2010-11-17 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 41.884144 | |
Longitude: -75.992358 |
Date | Event |
---|---|
2010-11-17 | New Permit Application |
2010-11-26 | Performed Spud Operation |
2011-01-23 | Drilling Completion |
2012-04-30 | DEVIATED |
For data sources see[4]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2012-01-27 | 2012-01-27 | 6,225 | 5,502,336 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | FRW-18 | Baker Hughes | Friction Reducer | Distillates, petroleum, hydrotreated light | 64742-47-8 | 30.00 | 0.03 | |
Sand, White, 30/50 | Baker Hughes | Proppant | Quartz | 14808-60-7 | 100.00 | 5.67 | ||
Sand, White, 100 mesh | Baker Hughes | Proppant | Quartz | 14808-60-7 | 100.00 | 1.64 | ||
Sand, White, 40/70 | Baker Hughes | Proppant | Quartz | 14808-60-7 | 100.00 | 6.79 | ||
InFlo 250W | Baker Hughes | Surfactant | Surfactants | 80.00 | 0.00050000 | |||
2-Butoxyethanol | 111-76-2 | 5.00 | 0.00003000 | |||||
Methanol | 67-56-1 | 30.00 | 0.00019000 | |||||
Hydrochloric Acid 10.1-15 | Baker Hughes | Acidizing | Hydrochloric acid | 7647-01-0 | 15.00 | 0.05 | ||
Water | 7732-18-5 | 85.00 | 0.30 | |||||
Scaletrol 720 | Baker Hughes | Scale Inhibitor | Ethylene glycol | 107-21-1 | 30.00 | 0.00459000 | ||
Calcium chloride | 10043-52-4 | 5.00 | 0.00077000 | |||||
Alpha 1427 | Baker Hughes | Biocide | Ethanol | 64-17-5 | 5.00 | 0.00112000 | ||
Quaternary ammonium compounds, benzyl-C12-16-alkyldimethyl, chlorides |
68424-85-1 | 5.00 | 0.00112000 | |||||
Didecyl dimethyl ammonium chloride | 7173-51-5 | 10.00 | 0.00223000 | |||||
Glutaraldehyde | 111-30-8 | 30.00 | 0.00670000 | |||||
Ferrotrol 300L | Baker Hughes | Iron Control | Citric acid | 77-92-9 | 60.00 | 0.00141000 | ||
Additional Ingredients | Baker Hughes | Surfactant | ||||||
Sorbitan Monooleate | ||||||||
Potassium chloride | 7447-40-7 | |||||||
Salt | ||||||||
Polyacrylate | ||||||||
Water | 7732-18-5 | |||||||
Sodium chloride | 7647-14-5 | |||||||
Poly (acrylamide-co-acrylic acid) | ||||||||
Ethoxylated Alcohol | ||||||||
Water | Operator | Carrier | Water | 7732-18-5 | 100.00 | 85.48 | ||
Additional Ingredients | Surfactant |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | CARRIZO (MARCELLUS) LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | CARRIZO (MARCELLUS) LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CARRIZO (MARCELLUS) LLC | 1,073,895.00 | 242 | 0.00 | 0 | 0.00 | 0 |
2013 | CARRIZO (MARCELLUS) LLC | 523,578.00 | 256 | 0.00 | 0 | 0.00 | 0 |
2014 | CARRIZO (MARCELLUS) LLC | 1,247.41 | 4 | 0.00 | 0 | 0.00 | 0 |
2015 | CARRIZO (MARCELLUS) LLC | 942,409.52 | 318 | 0.00 | 0 | 0.00 | 0 |
2016 | CARRIZO (MARCELLUS) LLC | 328,955.65 | 278 | 0.00 | 0 | 0.00 | 0 |
2017 | CARRIZO (MARCELLUS) LLC | 257,468.92 | 341 | 0.00 | 0 | 0.00 | 0 |
2018 | BKV OPR LLC | 194,500.89 | 363 | 0.00 | 0 | 0.00 | 0 |
2019 | BKV OPR LLC | 127,454.23 | 358 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2010 | CARRIZO (MARCELLUS) LLC | Drill Cuttings | 194.00 Tons | LANDFILL | NY31346244 |
2011 | CARRIZO (MARCELLUS) LLC | Drill Cuttings | 139.00 Tons | LANDFILL | NY31346244 |
2011 | CARRIZO (MARCELLUS) LLC | Drill Cuttings | 115.00 Tons | LANDFILL | NY # 02S17 |
2011 | CARRIZO (MARCELLUS) LLC | Drill Cuttings | 790.00 Tons | LANDFILL | 8-0728-0004/013 |
2011 | CARRIZO (MARCELLUS) LLC | Drilling Fluid Waste | 1,560.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2012 | CARRIZO (MARCELLUS) LLC | Drill Cuttings | 190.00 Tons | LANDFILL | NY STATE #32S11 |
2012 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 14,581.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2012 | CARRIZO (MARCELLUS) LLC | Drill Cuttings | 100.00 Tons | LANDFILL | THR029 |
2013 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 696.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2013 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 212.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NE003 |
2015 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 188.35 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2015 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 115.99 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC018 |
2015 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 153.44 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC010 |
2015 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 566.24 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NE003 |
2015 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 1,515.75 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | CARRIZO (MARCELLUS) LLC | Other Oil & Gas Wastes | 15.18 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2016 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 66.78 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2016 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 31.76 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123 |
2016 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 74.29 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NE003 |
2016 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 89.78 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC018 |
2016 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 107.99 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NE003 |
2016 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 33.91 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC010 |
2016 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 85.86 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2017 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 53.20 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2017 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 259.27 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC018 |
2017 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 45.50 Bbl | REUSE (AT WELL PAD) | |
2017 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 150.98 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NE003 |
2017 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 14.97 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123 |
2018 | BKV OPR LLC | Produced Fluid | 15.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NE003 |
2018 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 65.00 Bbl | REUSE (AT WELL PAD) | |
2018 | CARRIZO (MARCELLUS) LLC | Produced Fluid | 233.13 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC018 |
2019 | BKV OPR LLC | Produced Fluid | 15.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR119 |
2019 | BKV OPR LLC | Produced Fluid | 271.43 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC018 |
2019 | BKV OPR LLC | Produced Fluid | 15.00 Bbl | REUSE (AT WELL PAD) | |
2019 | BKV OPR LLC | Produced Fluid | 75.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NE003 |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2007324 | Primary Facility | 2011-09-29 | Routine/Complete Inspection | No Violations Noted | |
2014425 | Primary Facility | 2011-10-25 | Routine/Complete Inspection | Pending | DEP arrived on site at 11 am. The purpose of the inspection was to check the status of the wells and not any activity on site. At the time of inspection, crews were installing new plastic secondary containment for upcoming frac. Six wells have been drilled (1H - 6H). All six wells are currently shut in and not vented. Inspection of the Baker 4H cellar revealed steady bubbling between the 9 5/8" and 13 3/8" casing strings. It is requested by the DEP that the Operator identify the source of the leak. The Operator is to notify the DEP when this work is to be completed. The Operator shall provide a summary of the findings, and a description fo what repairs need to be completed. According to Chapter 78 Section 78.86...the Operator has the option to correct the defect or submit a plan to correct the defect for approval by the Department within 30 days. |
2038896 | Primary Facility | 2012-01-30 | Incident- Response to Accident or Event | Violation(s) Noted | |
2041359 | Primary Facility | 2012-02-07 | Follow-up Inspection | Pending | DEP on site 10 am to follow up on post fraccing incindent. Met with Steve Osborne and Chris Kyea of Carrizo. As per meeting with DEP and Carrizo, operator was to change assembly that failed on well heads and have Boots N Coots perform audit on well heads and frac equipment. New Companion flanges have been installed (molded) with true 10000 psi rating. Operator has re-torqued all bolts, cleaned grease pans on pumps, and cleaned up any spills or fluid associated with intial fraccing incident. Boots n Coots will be on site on Feb 8th to do audit. DEP will return on Feb 8th. At this time, no activity shall be performed at the site until approval from Department. |
2041367 | Primary Facility | 2012-02-08 | Follow-up Inspection | Pending | DEP on site 9 am. Met with Steve Osborne, Chris Kyea of Carrizo and Jason Alford and James Sothers of Boots & Coots. B & C on site to perform audit of frac equipment on site as result of recent frac incident. B& C completed audit at 11 am and submitted final report on site at approximately 12 am. Another B&C inspector will be on site later today to perform more Q5 inspection on well heads. At this time Carrizo still is to remain on standby until DEP approval is given to resume frac operations. DEP offsite 12 am. |
2053180 | Primary Facility | 2012-03-13 | Routine/Complete Inspection | No Violations Noted | Please refer to Baker 1H 3-13-12 inspection report regarding details of the investigation. Permit number is 115-20471. |
2077197 | Primary Facility | 2012-06-18 | Routine/Complete Inspection | Violation(s) Noted | See inspection report for full details |
2082735 | Primary Facility | 2011-01-11 | Drilling/Alteration | Violation(s) Noted | John Savage - company man. Nabors Rig M05. Currently at depth 6887'. Landed and now drilling lateral. Proposed TD - 12015'. 13 3/8" set at 680' and had no returns on cement job. Ran bond log to determine TOC. Did top job with 1" tremie and had returns. 9 5/8" set at 1805'. Had 35 bbls returned. BOPs passed. |
2082742 | Primary Facility | 2010-11-17 | Routine/Complete Inspection | No Violations Noted | |
2357039 | Primary Facility | 2015-04-01 | Routine/Complete Inspection | Pending | Cellar full of water with bubbling, test measures 100% LEL and 65% and building methane, no gauge on production casing, about 1200 lbs on tree top, vent pipe open and venting to tank at time of inspection, will request a vac truck be present while we are there to determine where the gas is coming from. |
2414155 | Primary Facility | 2015-10-08 | Follow-up Inspection | No Violations Noted | At time of inspection, arrived on site at 11:30 a.m., the wells were shut in with a crew working on the production line, met with Carrizo representatives Joe Sodon and Chris Lewis, Joe and Chris pumped water into the cellar to determine where the gas bubbles detected from the inspection on 4/1/15 were coming from. The water was pumped to a level above the (13x9) annulus with no gas bubbles detected. It was determined that the gas bubbles were coming from the (9x5) annulus, the (9x5) vent pipe was open and venting to a tank, there was 709psi on the production casing and 686psi on the production line. I took a walk around the site and everything looked OK. |
2451826 | Primary Facility | 2016-01-21 | Routine/Complete Inspection | No Violations Noted | The Department was on site to inspect the Baker well pad (ESX10-115-0029). The wells associated with the pad are as follows:
115-20471 115-20470 115-20469 115-20468 115-20467 115-20466 115-20465 The site was stable and well vegetated with no apparent erosional issues. There were no violations. If there are any issues please feel free to contact me |
2509564 | Primary Facility | 2016-07-28 | Routine/Complete Inspection | No Violations Noted | The Department was on site to inspect the Baker well pad (ESX10-115-0029). The wells associated with the pad are as follows:
115-20471 115-20470 115-20469 115-20468 115-20467 115-20466 115-20465 The site was stable and well vegetated with no apparent erosional issues. There were no violations. If there are any issues please feel free to contact me. |
2511743 | Primary Facility | 2016-08-17 | Site Restoration | No Violations Noted | The Department was on site to conduct a Notice of Termination on the Baker well pad (ESX10-115-0029 (1)). The wells associated with the pad are as follows:
115-20471 115-20470 115-20469 115-20468 115-20467 115-20466 115-20465 The site was rocky, but where there was enough soil for growth, vegetation was meeting or exceeding the 70% vegetative standard. There were a few remaining BMPs (silt sock) and these were promptly removed by Carrizo employees. Off the access road to the Impoundment and Well Site the landowner constructed an earthwork gun range, well vegetated and stable. This is causing no impact to the site or access road. The area was stable and had no erosional issues at this time and it is recommended that this Notice of Termination be APPROVED. There were no violations. If there are any issues please feel free to contact me. |
2512484 | Primary Facility | 2016-08-22 | Routine/Complete Inspection | No Violations Noted | At time of inspection, arrived on site at 13:00p.m., the cellar had water at the bottom with no bubbling noticed; the (9x5) vent pipe was open and venting into a tank. There was 493psi on the production casing and 1132psi on the production line. I took a walk around the location and everything looked OK.
I left the site at 13:40p.m. |
2606525 | Primary Facility | 2017-06-21 | Routine/Complete Inspection | No Violations Noted | At time of inspection, arrived on site at 10:35a.m.
The cellar was full of water with bubbling noticed. Gas was detected at 100% LEL and peaked at 16% methane. It was determined that the bubbling was coming from the (9x5) annulus during an inspection (IR#2414155) conducted on 10/8/15. The (9x5) annulus vent pipe was open and venting into the production tank. There was 459psi on the production casing and 450psi on the production line. I took a walk around the location and there were no obvious concerns noticed. I left the site at 11:20a.m. |
2713027 | Primary Facility | 2018-03-28 | Routine/Complete Inspection | No Violations Noted | At time of inspection.
The well was in production. There was water 3' below grade in the cellar with no bubbling noticed and no gas detected in the remainder of the cellar. I took a walk around the location and there were no obvious concerns noticed. There were no violations noted. |
2817034 | Primary Facility | 2018-12-18 | Routine/Complete Inspection | No Violations Noted | At time of inspection.
The well was in production. The cellar was empty and there was no gas detected with a MSA Altair 5X multi gas detector that was calibrated on 12/3/18. The permit number for the 4H on the entrance sign was incorrect (see photo #2). It was 155-20468 and should be 115-20468. I contacted Jesse Bonnice of BKV to have it corrected. I took a walk around the location and there were no obvious concerns noticed. There were no violations noted. |
2851757 | Primary Facility | 2019-03-11 | Routine/Complete Inspection | No Violations Noted | I performed a Routine Complete (RTNC) inspection of the Baker Well Pad on March 11, 2019. The weather was sunny and relatively warm, around 38 degrees.
The access road was a bit muddy but not unstable. The access road is quite long, passing some small logging operations, as well as a target shooting range situated along its length. The well pad surface was plowed and mostly wet but stable. The wellheads were encased in a carport structure. They were surrounded by clean gravel and were properly labeled. The containment surrounding the production tanks and apparatus was mostly empty and had sufficient freeboard. The cut and fill slopes of the site were rocky and stable. Where there was sufficient soil, there was adequate vegetation. No areas of instability were noted. The impoundment on site was full to capacity. It would be recommended to draw down the impoundment to prevent overflow and possible resulting E&S issues. There were no violations noted |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2038896 | 630934 | 01/30/2012 | 2012-01-30 | 78.56PITCNST - Impoundment not structurally sound, impermeable, 3rd party protected, greater than 20" of seasonal high ground water table | Administrative | |
2038896 | 630940 | 01/30/2012 | 2012-01-30 | SWMA301 - Failure to properly store, transport, process or dispose of a residual waste. | Environmental Health & Safety | |
2038896 | 630941 | 01/30/2012 | 2012-01-30 | 402CSL - Failure to adopt pollution prevention measures required or prescribed by DEP by handling materials that create a danger of pollution. | Environmental Health & Safety | |
2038896 | 630942 | 01/30/2012 | 2012-01-30 | 78.73A - Operator shall prevent gas and other fluids from lower formations from entering fresh groundwater. | Environmental Health & Safety | |
2077197 | 642171 | 06/18/2012 | 2012-06-18 | 402CSL - Failure to adopt pollution prevention measures required or prescribed by DEP by handling materials that create a danger of pollution. | Environmental Health & Safety | |
2077197 | 642172 | 06/18/2012 | 2012-06-18 | 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. | Environmental Health & Safety | |
2082735 | 643768 | 01/11/2011 | 2011-01-11 | 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
630934 | 280092 | NOV - Notice of Violation | Comply/Closed | 2012-12-26 | |||
630934 | 292339 | CACP - Consent Assessment of Civil Penalty | Comply/Closed | 2012-12-26 | 2012-12-26 | $73,271.00 | $73,271.00 |
630940 | 280092 | NOV - Notice of Violation | Comply/Closed | 2012-12-26 | |||
630940 | 292339 | CACP - Consent Assessment of Civil Penalty | Comply/Closed | 2012-12-26 | 2012-12-26 | $73,271.00 | $73,271.00 |
630941 | 280092 | NOV - Notice of Violation | Comply/Closed | 2012-12-26 | |||
630941 | 292339 | CACP - Consent Assessment of Civil Penalty | Comply/Closed | 2012-12-26 | 2012-12-26 | $73,271.00 | $73,271.00 |
630942 | 280092 | NOV - Notice of Violation | Comply/Closed | 2012-12-26 | |||
630942 | 292339 | CACP - Consent Assessment of Civil Penalty | Comply/Closed | 2012-12-26 | 2012-12-26 | $73,271.00 | $73,271.00 |
For data sources see[8]