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37-115-21142

Well Details

Well ID: 37-115-21142
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Country: United States
State: Pennsylvania
County: Susquehanna
Municipality: New Milford Township
Operator Name: SWN PROD CO LLC
Well Pad ID: 144552
Farm/Lease Name: FOLGER 5H
License Status:
Spud Date:
Permit Date: 2013-02-04
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.827558
Longitude: -75.742397

For data sources see[1][2][3]

Well History

Date Event
2013-02-04 New Permit Application
2013-03-15 Performed Spud Operation
2013-05-09 Drilling Completion
2013-05-28 Perforation
2013-06-05 Performed Stimulation
2015-03-10 DEVIATED

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2013-06-05 2013-06-09 5,392 7,579,030

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 15% HCl Keane Acid HCL 7647-01-0 15 0.012965 0
Water SWN Water / Produced Water H2O + Dissolved Salts 7732-18-5 100 89.9305 0
Sand Keane Proppant Crystalline Silica, Quartz 14808-60-7 100 9.11896 0
FRA-405 Clearwater Friction Reducer Sodium Chloride 7647-14-5 10 0.00616 0
Petroleum Distillates 64742-47-8 40 0.02465 0
Ammonium Chloride 12125-02-9 7 0.00431 0
Alcohols, C-12-16, Ethoxylated 68551-12-2 7 0.00431 0
AI-250 Clearwater Acid Inhibitor Isopropanol 67-63-0 40 0.00086 0
Glycol Ethers 111-76-2 40 0.00086 0
Propargyl Alcohol 107-19-7 40 0.00086 0
Ethoxylated Nonylphenol 68412-54-4 13 0.00028 0
EC6486A Nalco Scale Inhibitor Ethylene Glycol 107-21-1 30 0.00307 0
Bio Clear 2000 Weatherford Biocide Dibromoacetonitrile 3252-43-5 5 0.00061 0
2,2-Dibromo-3-nitrilopropionamide 10222-01-2 30 0.00365 0

For data sources see[5]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
2013-06-05 0 0 0

For data sources see[6]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2013 SOUTHWESTERN ENERGY PROD CO 634,214.00 122 0.00 0 0.00 0
2014 SOUTHWESTERN ENERGY PROD CO 1,945,208.00 362 0.00 0 0.00 0
2015 SWN PROD CO LLC 1,519,041.00 365 0.00 0 0.00 0
2016 SWN PROD CO LLC 1,183,589.00 366 0.00 0 0.00 0
2017 SWN PROD CO LLC 787,954.00 365 0.00 0 0.00 0
2018 SWN PROD CO LLC 779,214.00 365 0.00 0 0.00 0
2019 SWN PROD CO LLC 898,715.00 365 0.00 0 0.00 0

For data sources see[7]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2013 SOUTHWESTERN ENERGY PROD CO Fracing Fluid Waste 10,919.00 Bbl REUSE OTHER THAN ROAD SPREADING
2013 SOUTHWESTERN ENERGY PROD CO Drill Cuttings 1,438.14 Tons LANDFILL 101247
2013 SOUTHWESTERN ENERGY PROD CO Produced Fluid 4,624.00 Bbl REUSE OTHER THAN ROAD SPREADING
2014 SOUTHWESTERN ENERGY PROD CO Produced Fluid 3,412.00 Bbl REUSE OTHER THAN ROAD SPREADING
2015 SWN PROD CO LLC Produced Fluid 972.75 Bbl REUSE OTHER THAN ROAD SPREADING
2016 SWN PROD CO LLC Other Oil & Gas Wastes 35.00 Bbl REUSE OTHER THAN ROAD SPREADING
2016 SWN PROD CO LLC Produced Fluid 615.00 Bbl REUSE OTHER THAN ROAD SPREADING
2017 SWN PROD CO LLC Other Oil & Gas Wastes 50.00 Bbl SURFACE IMPOUNDMENT 95-16-65420-013
2017 SWN PROD CO LLC Produced Fluid 170.00 Bbl SURFACE IMPOUNDMENT 95-16-65420-013
2018 SWN PROD CO LLC Produced Fluid 460.25 Bbl SURFACE IMPOUNDMENT 95-16-65420-013
2018 SWN PROD CO LLC Produced Fluid 58.50 Bbl REUSE (AT WELL PAD)
2018 SWN PROD CO LLC Other Oil & Gas Wastes 177.83 Bbl SURFACE IMPOUNDMENT 95-16-65420-013
2018 SWN PROD CO LLC Produced Fluid 93.25 Bbl SURFACE IMPOUNDMENT 826342
2019 SWN PROD CO LLC Produced Fluid 57.50 Bbl SURFACE IMPOUNDMENT 826342
2019 SWN PROD CO LLC Other Oil & Gas Wastes 37.04 Bbl SURFACE IMPOUNDMENT 95-16-65420-013
2019 SWN PROD CO LLC Produced Fluid 243.25 Bbl SURFACE IMPOUNDMENT 95-16-65420-013

For data sources see[8]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2152511 Primary Facility 2013-03-29 Routine/Partial Inspection No Violations Noted
2174000 Primary Facility 2013-05-07 Drilling/Alteration No Violations Noted 20-75'
2174017 Primary Facility 2013-03-27 Drilling/Alteration No Violations Noted NE11 - Rigging up to drill Folger 5H
2208551 Primary Facility 2013-09-24 Routine/Complete Inspection No Violations Noted Refer to inspection ID # 2208531
2208801 Primary Facility 2013-09-24 Routine/Complete Inspection No Violations Noted Refer to inspection ID # 2208782
2260929 Primary Facility 2014-04-08 Routine/Complete Inspection No Violations Noted On 4/8/14, the Department conducted a follow-up inspection of SWN RU 32 Folger Pad where violations had been noted by the Department during a 9/24/13 inspection. The cut slope has been effectively stabilized. As of this inspection, violations noted in the 9/24/13 inspection have been corrected/abated.
2359314 Primary Facility 2015-04-07 Routine/Complete Inspection No Violations Noted
2477441 Primary Facility 2016-04-22 Routine/Complete Inspection No Violations Noted
2488552 Primary Facility 2016-05-31 Routine/Complete Inspection No Violations Noted
2558052 Primary Facility 2017-02-01 Routine/Complete Inspection No Violations Noted At time of inspection, arrived on site at 15:25p.m., the cellar was full of gravel and there was no gas detected at the perimeter of the cellar. The vent pipe was open and set up with a Taylor plug to check for pressure and the valve going to the production tank was closed. There was 678psi on the production casing and 515psi on the production line. I took a walk around the location and noticed that the entire site was covered with snow except a section between the production tanks and the production units. I contacted Gene Rickard (DEP WQS) to let him know about the well site.

I left the site at 16:05p.m.

2564081 Primary Facility 2017-02-02 Routine/Complete Inspection No Violations Noted Today’s inspection was conducted after a Department Oil and Gas Inspector noticed a large area of unfrozen standing water on the well pad surface near the production tanks and production units. The unfrozen water is unusual in respect to the fact that recent and current temperatures have been and are well below freezing. The Department employed an Extech Instruments ExStik 2 Conductivity Meter, tested the water and found the conductivity to be around 90 microsiemens, a relatively low number. Of note is the fact that algae was present and thriving in the standing water. The presence of the algae suggests that the water is probably an expression of ground water which would also explain the temperatures recorded of the standing water of 9 degrees Celsius. Overall, the pad site looked good with no E&S violations observed.
2564098 Primary Facility 2017-02-06 Routine/Complete Inspection No Violations Noted Today’s inspection is being conducted after having consulted with a Department Geologist and a Department Oil and Gas Inspector in reference to the standing water observed on the SWN RU 32 Folger Pad. The consensus was that it would be prudent for the Department to collect samples, soil and water, of the standing unfrozen water and associated contact soil on the pad to ensure that the presence of the standing unfrozen water is a natural phenomenon. Present during the inspection was myself, Jon Sassi, Department EPS, Eric Rooney, Department LPG, David Schoonover, Department OGI, and Mike Deming, SWN Senior Regulatory Analyst. Mr. Deming did state that SWN has always been aware of the standing water and that its presence has been attributed to the theory that the water is a natural expression of ground water. The Department collected 3 separate samples, one soil sample and two water samples. The soil sample, 0257238, will be tested for glycol and methanol. One of the water samples, 0257239 will be tested
2651851 Primary Facility 2017-10-25 Routine/Complete Inspection No Violations Noted At time of inspection.

The well was in production. The cellar was full of gravel and there was no gas detected at the perimeter of the cellar. I took a walk around the location and there were no obvious concerns noticed. There were no violation noted.

2753329 Primary Facility 2018-07-18 Routine/Complete Inspection No Violations Noted At time of inspection.

The well was in production. The cellar was full of gravel and there was no gas detected at the perimeter of the cellar. I took a walk around the location and there were no obvious concerns noticed. There were no violations noted.

2855690 Primary Facility 2019-03-19 Routine/Complete Inspection No Violations Noted At time of inspection.

The well was in production. The cellar was full of gravel and there was no gas detected at the perimeter of the cellar with a MSA Altair 5X multi gas detector that was calibrated on 3/4/19. I took a walk around the location and there were no obvious concerns noticed. There were no violations noted.

For data sources see[9]

References