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Well ID: 37-125-01330 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Washington | |
Municipality: Fallowfield Township | |
Operator Name: VIKING RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: J YANKOSKY 670653 | |
License Status: PLUGGED & ABANDONED | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.142392 | |
Longitude: -79.976842 |
Date | Event |
---|---|
1923-08-15 | Drilling Completion |
1986-07-22 | OLD WELL |
2015-06-26 | Drilling Completion |
2016-06-07 | FULLY PLUGGED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | COLUMBIA NATURAL RES INC | 1.00 | 21 | 0.00 | 0 | 0.00 | 0 |
1998 | CASTLE GAS CO INC | 113 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | CASTLE GAS CO INC | 56 | 348 | 0.00 | 0 | 0.00 | 0 |
2000 | CASTLE GAS CO INC | 39 | 351 | 0.00 | 0 | 0.00 | 0 |
2001 | VIKING RESOURCES CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2002 | VIKING RESOURCES CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2003 | VIKING RESOURCES CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2004 | VIKING RESOURCES CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2005 | VIKING RESOURCES CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2006 | VIKING RESOURCES CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | VIKING RESOURCES CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | VIKING RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2415880 | Primary Facility | 2015-06-22 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Nick's Well Plugging pulled tubing OOH, TIH w/ open-ended tubing and washed down to 2670 feet (well had been plugged back to ~2600 feet in 1967). Called attainable bottom @2670 feet and spotted cement plug up to 2225 feet. |
2415892 | Primary Facility | 2015-06-23 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Wireline company ran bond log on 4" casing, shot collar above free point @1469 feet. Nick's Well Plugging pulled 4" casing. Wireline company ran bond log on 6 5/8" casing, shot collar above free point @1003 feet. After several attempts 6 5/8" casing began to pull free (photo). |
2415905 | Primary Facility | 2015-06-24 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Nick's Well Plugging pulled all 1003 feet of 6 5/8" casing OOH. Latched onto 8 1/4" casing and attempted several times to pull, but would not come, no stretch. wireline truck scheduled for next morning. |
2415933 | Primary Facility | 2015-06-25 | Plugging(Includes Plugged/Mined Through) | In Compliance with Schedule | Wireline company ran bond log on 8 1/4" casing, found tight spots all along casing to surface. They cut collar @ 948 feet after perfing several depths below. Nick's Well Plugging attempted to pull casing, but could not. Wireline company perfed remaining casing at several depths to prepare to cement to surface. Nick' TIH w/ cement string, hit obstruction, TOOH. TIH w/ bit, cleaned out obstruction. |
For data sources see[6]