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| Well ID: 37-125-01707 | Loading map...
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| Country: United States | |
| State: Pennsylvania | |
| County: Washington | |
| Municipality: Cecil Township | |
| Operator Name: PA TURNPIKE COMM | |
| Well Pad ID: | |
| Farm/Lease Name: PLUNKETT | |
| License Status: Plugged and Abandoned | |
| Spud Date: | |
| Permit Date: | |
| Well Type: GAS | |
| Unconventional Well: N | |
| Configuration: Vertical Well | |
| Conservation: No | |
| Latitude: 40.307281 | |
| Longitude: -80.152831 |
| Date | Event |
|---|---|
| 1901-01-01 | Drilling Completion |
| 1988-10-03 | OLD WELL |
| 2019-01-09 | Begin Plugging |
| 2019-01-24 | Finished Plugging |
| 2020-02-14 | Fully Plugged |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
|---|---|---|---|---|---|---|---|
| 2009 | ONEXXX PROD & EXPLORATION CORP | 1,218.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2010 | ONEXXX PROD & EXPLORATION CORP | 1,121.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2011 | ONEXXX PROD & EXPLORATION CORP | 438.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2012 | ONEXXX PROD & EXPLORATION CORP | 612.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2013 | ONEXXX PROD & EXPLORATION CORP | 358.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2014 | ONEXXX PROD & EXPLORATION CORP | 235.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2015 | ONEXXX PROD & EXPLORATION CORP | 223.00 | 365 | 0.00 | 0 | 0.00 | 0 |
| 2016 | ONEXXX PROD & EXPLORATION CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2017 | ONEXXX PROD & EXPLORATION CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
| Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|---|
| 2778950 | Primary Facility | 2018-09-24 | Routine/Partial Inspection | No Viols - Fac Inactive for Inspection | Visited site of this shut in well (Beltway well #C2-2.1) to check status of recent repairs (9/7/18) by Yost per request of Turnpike Commission. This well may have been damaged by vandals who appear to have twisted the production casing and caused flow line to part. A leak was created in the annulus of the production casing-surface casing that Yost successfully repaired by filling annulus with concrete until well can be plugged. A low volume of gas is leaking past closed valve on parted flowline. |
| 2830416 | Primary Facility | 2019-01-04 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Road into well and small pad built for rig mobilization next week. |
| 2830940 | Primary Facility | 2019-01-14 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost attempted repeatedly to pull 3" from well, but 7" also coming. Loggers scheduled to perf bottom 200' of 3" so bottom hole plug can be set. |
| 2830953 | Primary Facility | 2019-01-16 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost pulling 3" after cutting collar at 1753'. Have about 30 joints out so far. First joint had a 3' section of 7" attached. The 7" was rusted off of remaining string left in well. |
| 2831009 | Primary Facility | 2019-01-17 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | TIMCO ran ccl/caliper log, found 6 5/8" casing down to 1542'. Will perf to surface. |
| 2831024 | Primary Facility | 2019-01-22 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost warming up equipment, rig won't start (temperature is zero degrees). Set 60 sack plug last Friday. Will tag TOC and pump next plug later today. |
| 2831114 | Primary Facility | 2019-01-24 | Plugging(Includes Plugged/Mined Through) | In Compliance with Policy | Yost plugged well to surface. Rig stacked off location nearby. Demobilizing. |
For data sources see[6]