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37-125-01852

Well Details

Well ID: 37-125-01852
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Country: United States
State: Pennsylvania
County: Washington
Municipality: South Franklin Township
Operator Name: LEATHERWOOD INC
Well Pad ID:
Farm/Lease Name: SARAH J. CRACRAFT 1
License Status: PLUGGED & ABANDONED
Spud Date:
Permit Date:
Well Type: OIL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.090733
Longitude: -80.328081

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
1901-01-01 OLD WELL
2011-09-30 Drilling Completion
2013-06-26 FULLY PLUGGED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2004 MASON STEPHEN L 0.00 0 5 365 0.00 0
2005 MASON STEPHEN L 0.00 0 40 365 0.00 0
2006 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0
2007 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0
2008 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0
2009 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0
2010 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0
2011 LEATHERWOOD INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1003570 Primary Facility 2001-02-08 Compliance Evaluation No Violations Noted Checked this well after spill clean-up and during ongoing absorbtion of residual oil. Petro-clean has done an adequate job of working to minimize spill damage in the use of absorbents, haybales, and associated mop-up. Later, soil remediation and improved diking at tank site is expected with the return of fairer weather .... for the purposes of soil remediation and better containment.
1028775 Primary Facility 2001-05-08 Routine/Complete Inspection No Violations Noted Tank & clean-up completed, fresh soil mulched, sheen eliminated.
2018627 Primary Facility 2011-10-11 Incident- Response to Accident or Event Violation(s) Noted
2032526 Primary Facility 2011-10-24 Follow-up Inspection No Violations Noted
2034594 Primary Facility 2012-01-03 Compliance Evaluation No Violations Noted
775900 Primary Facility 1997-11-06 Routine/Complete Inspection Violation(s) Noted NO TAG (RGSTR)/ABAND & UNPLGGD
999265 Primary Facility 2001-01-30 Complaint Inspection Violation(s) Noted Overtopped tank discharge, timer assembly problem possible on pump cut-off, etc. Diking not holding crude oil overtopping. Also, measures to prevent spill not taken, re: permeable diking, poorly maintained. Thirdly, discharge of I. w. (crude oil & brine) to stream - inadequate prevention & overall containment.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2018627 624526 10/11/2011 2011-10-11 301CSL - Stream discharge of IW, includes drill cuttings, oil, brine and/or silt Environmental Health & Safety ~1bbl of crude oil releaed during plugging operation. Cited in NOV - CSL 301/307, SWMA 301, O&G 78.54 and 78.60 (a)
2018627 624527 10/11/2011 2011-10-11 91.33A - Failure to notify DEP of pollution incident. No phone call made forthwith Administrative Incident occurred ~ 1 - 1&1/2 weeks prior to notification. Coastal drilling (subcontractor) notified CNX/Consol on 10/7/11 (1 - 1&1/2 wks after incident); voice message to Don Rugh on 10/10/11 (Columbus Day); Consol notified live person on 10/11/11.
775900 110534 11/06/1997 1997-11-06 203TAG - Failure to affix, in a permanent manner, a registration number on a well within 60 days of registration Administrative NO TAG (RGSTR)
775900 110535 11/06/1997 1997-11-06 210A - Failure to adequately plug or schedule plugging of a well upon abandonment Administrative ABAND & UNPLUGGED
999265 259854 01/30/2001 2001-01-30 401 CSL - Discharge of pollultional material to waters of Commonwealth. Environmental Health & Safety
999265 259855 01/30/2001 2001-01-30 691.1 - Clean Streams Law-General. Used only when a specific CLS code cannot be used Administrative
999265 259856 01/30/2001 2001-01-30 301CSL - Stream discharge of IW, includes drill cuttings, oil, brine and/or silt Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
624526 277058 NOV - Notice of Violation
624526 281991 CACP - Consent Assessment of Civil Penalty Comply/Closed 2012-03-30 2012-03-30 $9,900.00 $9,900.00
624527 277058 NOV - Notice of Violation
624527 281991 CACP - Consent Assessment of Civil Penalty Comply/Closed 2012-03-30 2012-03-30 $9,900.00 $9,900.00
110534 6951 NOV - Notice of Violation Legacy Data 1999-09-13
110535 6951 NOV - Notice of Violation Legacy Data 1999-09-13
259854 59992 NOV - Notice of Violation Comply/Closed 2001-02-20
259855 59992 NOV - Notice of Violation Comply/Closed 2001-02-20
259856 59992 NOV - Notice of Violation Comply/Closed 2001-02-20

For data sources see[6]

References