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37-125-23877

Well Details

Well ID: 37-125-23877
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Country: United States
State: Pennsylvania
County: Washington
Municipality: Independence Township
Operator Name: RANGE RESOURCES APPALACHIA LLC
Well Pad ID: 148422
Farm/Lease Name: GOETTEL UNIT 13H
License Status: PLUGGED & ABANDONED
Spud Date:
Permit Date: 2009-10-15
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 40.240111
Longitude: -80.464750

For data sources see[1][2][3]

Well History

Date Event
2009-10-15 New Permit Application
2009-12-14 Performed Spud Operation
2010-01-24 Drilling Completion
2010-01-26 Drilling Completion
2010-04-23 NEWLY DRILLED
2010-10-15 FULLY PLUGGED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2009 RANGE RESOURCES APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2010 RANGE RESOURCES APPALACHIA LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 RANGE RESOURCES APPALACHIA LLC Drilling Fluid Waste 208.50 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 301353

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1851408 Primary Facility 2009-12-15 Drilling/Alteration No Violations Noted Well spud, Cellar in and 40' - 26" set
1859696 Primary Facility 2010-01-25 Drilling/Alteration No Violations Noted Rig Whipstock 24 - Fishing for hammer, stabilizer and 1 collar , Fish still in the hole , red rock swelling and caving in on tools. After 5 failed attempts and losing depth. Operated requested to plug well @ 630 to surface with cement. Verbal authorization granted by D Rugh
1859698 Primary Facility 2010-01-21 Drilling/Alteration No Violations Noted Rig Whipstock 24 - Circulation and return on 20", Pin twisted off , Fishing for hammer, stabilizer and 1 collar.
2751111 Primary Facility 2018-07-12 Incident- Response to Accident or Event In Compliance with Policy On 7/12/18 an incident inspection was conducted at the Goettel Unit Well Site in response to a spill reported on 6/29/18 by the operator. The following was observed:

>>The initial report stated that 20 gallons of produced water spilled around the well head.

>>Communication with operator personal at the time of inspection indicated that the spill occurred while servicing the well missing containment on site, the crew on site began cleanup immediately. Materials were placed into three roll off boxes and disposed. Cleanup was completed that day.

>>Site inspection found no indication of ongoing or unremediated issues. Cleanup appears to be in compliance with policy.

For data sources see[7]

References