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34-103-21649

Well Details

Well ID: 34-103-21649
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Country: United States
State: Ohio
County: Medina
Municipality: Sharon Township
Operator Name: KING DRILLING CO
Well Pad ID:
Farm/Lease Name: MAUCH
License Status: Plugged and Abandoned
License Date: 2015-04-09
Spud Date: 1967-07-19
Spud Drilling Contractor:
Final Drill Date: 1967-08-24
Well Total Depth: 3602.00 ft
Configuration: Vertical
Latitude: 41.100000
Longitude: -81.750000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1967-05-19 255 KING DRILLING CO GeoDate 5/19/67
Original Spud 1967-07-19
Completed 1967-08-24
Reached Total Depth 1967-08-24
APP 2015-04-09 Proposed Formations:CLINTON, Issued Date:4/9/2015, Expired Date:4/8/2017 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-12-01
Construction Permit Expires 2016-04-08
Record Last Modified 2017-02-10

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1200 Bbl 31500

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 KING DRILLING CO 446.00 0.00 0
1985 KING DRILLING CO 406.00 0.00 0
1986 KING DRILLING CO 589.00 0.00 365
1993 KING DRILLING CO 82.00 20.00 365
1995 KING DRILLING CO 20.00 16.00 365
1996 KING DRILLING CO 0.00 14.00 365
1997 KING DRILLING CO 48.00 15.00 365
1998 KING DRILLING CO 93.00 0.00 365
1999 KING DRILLING CO 181.00 19.00 365
2000 KING DRILLING CO 156.00 11.00 365
2001 KING DRILLING CO 37.00 14.00 365
2002 KING DRILLING CO 216.00 16.00 365
2003 KING DRILLING CO 84.00 0.00 365
2004 KING DRILLING CO 66.00 0.00 365
2005 KING DRILLING CO 0.00 0.00 365
2006 KING DRILLING CO 0.00 0.00 365
2007 KING DRILLING CO 0.00 0.00 365
2008 KING DRILLING CO 0.00 0.00 365
2009 KING DRILLING CO 0.00 0.00 365
2010 KING DRILLING CO 0.00 0.00 365
2011 KING DRILLING CO 0.00 0.00 365
2012 KING DRILLING CO 0.00 0.00 366
2013 KING DRILLING CO 0.00 0.00 365
2014 KING DRILLING CO 0.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 KING DRILLING CO Brine 0 0
1985 KING DRILLING CO Brine 0 0
1986 KING DRILLING CO Brine 0 365
1993 KING DRILLING CO Brine 0 365
1995 KING DRILLING CO Brine 0 365
1996 KING DRILLING CO Brine 0 365
1997 KING DRILLING CO Brine 0 365
1998 KING DRILLING CO Brine 23 365
1999 KING DRILLING CO Brine 0 365
2000 KING DRILLING CO Brine 0 365
2001 KING DRILLING CO Brine 94 365
2002 KING DRILLING CO Brine 97 365
2003 KING DRILLING CO Brine 0 365
2004 KING DRILLING CO Brine 14 365
2005 KING DRILLING CO Brine 0 365
2006 KING DRILLING CO Brine 0 365
2007 KING DRILLING CO Brine 0 365
2008 KING DRILLING CO Brine 0 365
2009 KING DRILLING CO Brine 0 365
2010 KING DRILLING CO Brine 0 365
2011 KING DRILLING CO Brine 0 365
2012 KING DRILLING CO Brine 0 366
2013 KING DRILLING CO Brine 0 365
2014 KING DRILLING CO Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1391472056 2015-11-4 0:00: PW No Violations 3.00
-52633136 2015-4-23 0:00: PW No Violations
0052633136 2015-04-23 Production Wells No Violations Inspected production well on 04/23/2015 to follow-up on a previously-issued compliance notice. The tank battery consists of 1-100 bbl steel tanks and 1-vertical separator located within an earthen dike. The tank battery is used by multiple wells (2); well identification is clearly displayed for all wells utilizing it. The well is equipped with a pump jack with a gas-powered motor. No identification is posted at the wellhead as required. A written request for a 6-month extension to the compliance notice was received from Andrew King (King Drilling), and a plugging permit was issued 04/09/2015. A 6-month extension is granted to allow King Drilling additional time to get the well plugged.
0226592472 2015-12-01 Production Wells No Violations The well was plugged 12/01/2015. Please see plugging report for additional information. As the well has been plugged, the compliance notice can be closed out.
1391472056 2015-11-04 Production Wells No Violations The operator is plugging the well. Norburt Lowder and Allie Sherwood of ODNR were unable to witness setting the bottom plug. On arrival to the location, the operator advised that cement had been postponed due to problems with the well. The service rig was pulling rods from the well and was planning on steaming out the tubing due to paraffin buildup. A pit was constructed to steam tubing into. No GPS was taken at the wellhead due to service rig operation.
1555554804 2015-11-10 Plug / Plug Back No Violations Thompson Well Service was on location from 11/04/2015-11/10/2015 attempting get downhole in order to plug the well. The tubing is hung uphole in the hole, and was plugged off with paraffin, however multiple solvent treatments have allowed some movement of the rods downhole. Andrew King with King Drilling requested an extension to the compliance notice for time to come up with a plan to properly well, and the extension was granted.
1611315985 2014-09-03 Production Wells Violations Noted Inspected production well on 09/03/2014. The tank battery consists of 1-100 bbl steel tank and 1-vertical separator located within a very overgrown earthen dike. The tank battery is used by multiple wells (2); well identification is clearly displayed for all wells utilizing it. The well is equipped with a pump jack with a hitmiss motor; the area around the wellhead is very overgrown. No well identification is posted at the wellhead as required. Research into the production history of the well showed that it has not produced since 2004, nor met the minimum production requirements since 2002, therefore the well must be plugged.
226592472 2015-12-1 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1611315985 US-OH-115819 2014-10-07 Failure to legibly identify well
1611315985 US-OH-115820 2014-10-07 Well shall be plugged

For data sources see[8]

References