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34-169-22054

Well Details

Well ID: 34-169-22054
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Country: United States
State: Ohio
County: Wayne
Municipality: Baughman Township
Operator Name: JAMES R BERNHARDT INC
Well Pad ID:
Farm/Lease Name: HAMMER-GRABER
License Status: Final Restoration
License Date: 2003-07-11
Spud Date: 1978-07-25
Spud Drilling Contractor: RUPP DRILLING
Final Drill Date: 1978-10-13
Well Total Depth: 3768.00 ft
Configuration: Vertical
Latitude: 40.890000
Longitude: -81.740000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-06-01 120 BERNHARDT JAMES R INC GeoDate 6/1/78
Original Spud 1978-07-25
Completed 1978-10-13
Reached Total Depth 1978-10-13
Completion Report Received 1979-04-17
APP 2003-07-11 Proposed Formations:CLINTON, Issued Date:7/11/2003, Expired Date:7/10/2004 6:00:00 AM, Drilling unit acres:68, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2003-12-17
Construction Permit Expires 2004-07-10
Record Last Modified 2017-02-15

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 91000 Gal 30000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 SCHRIMSHER OIL & GAS EXPL 5389.00 0.00 0
1985 SCRIMGEOUR ROBERT 4537.00 70.00 0
1986 SCRIMGEOUR ROBERT 3732.00 0.00 365
1987 SCHRIMSHER OIL & GAS EXPL 1074.00 0.00 365
1988 SCHRIMSHER OIL & GAS EXPL 0.00 0.00 365
1989 SCHRIMSHER OIL & GAS EXPL 0.00 0.00 365
1990 JAMES R BERNHARDT INC 0.00 0.00 0
1991 JAMES R BERNHARDT INC 0.00 0.00 365
1992 JAMES R BERNHARDT INC 0.00 0.00 365
1993 JAMES R BERNHARDT INC 0.00 0.00 0
1994 JAMES R BERNHARDT INC 0.00 0.00 365
1995 JAMES R BERNHARDT INC 0.00 0.00 0
1996 JAMES R BERNHARDT INC 0.00 0.00 0
1997 JAMES R BERNHARDT INC 0.00 0.00 0
1999 JAMES R BERNHARDT INC 0.00 0.00 0
2000 JAMES R BERNHARDT INC 0.00 0.00 0
2001 JAMES R BERNHARDT INC 0.00 0.00 365
2002 JAMES R BERNHARDT INC 0.00 0.00 0
2003 JAMES R BERNHARDT INC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 SCHRIMSHER OIL & GAS EXPL Brine 0 0
1985 SCRIMGEOUR ROBERT Brine 0 0
1986 SCRIMGEOUR ROBERT Brine 0 365
1987 SCHRIMSHER OIL & GAS EXPL Brine 0 365
1988 SCHRIMSHER OIL & GAS EXPL Brine 0 365
1989 SCHRIMSHER OIL & GAS EXPL Brine 0 365
1990 JAMES R BERNHARDT INC Brine 0 0
1991 JAMES R BERNHARDT INC Brine 0 365
1992 JAMES R BERNHARDT INC Brine 40 365
1993 JAMES R BERNHARDT INC Brine 0 0
1994 JAMES R BERNHARDT INC Brine 0 365
1995 JAMES R BERNHARDT INC Brine 0 0
1996 JAMES R BERNHARDT INC Brine 0 0
1997 JAMES R BERNHARDT INC Brine 0 0
1999 JAMES R BERNHARDT INC Brine 0 0
2000 JAMES R BERNHARDT INC Brine 0 0
2001 JAMES R BERNHARDT INC Brine 0 365
2002 JAMES R BERNHARDT INC Brine 0 0
2003 JAMES R BERNHARDT INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1236019352 2003-12-11 0:00 PB No Violations 1.50
-1788874677 2003-11-28 0:00 PB No Violations 1.20
-702249199 2003-12-24 0:00 PB No Violations 1.00
-908656274 2003-11-4 0:00: PB No Violations 1.00
-996622150 2003-12-15 0:00 PB No Violations 4.00
0054208147 2004-09-02 Final Restoration No Violations Meets requirements for restoration final.
0702249199 2003-12-24 Plug / Plug Back No Violations My inspection showed that the cement at the top of this well had settled and additional cement is needed to fill to surface.
0908656274 2003-11-04 Plug / Plug Back No Violations Check on progress of well plugging . The operator has service rig over the hole fishing for tubing. They are at 124ft.
0996622150 2003-12-15 Plug / Plug Back No Violations Try and set plug at 2300 ft. and could not get shot line down hole. Pick up tools and go back in and try and clear pipe / could not and went out to plug front well on this lease while Glen Davis works on well.
1070307762 2003-11-21 Plug / Plug Back No Violations Check on rig status for plugging of well with bad casing and tubing. Today they are fishing for chunks of shreded casing and tubing. Still pulling junk out at 124 ft.
1071586956 2003-12-02 Plug / Plug Back No Violations Check on rig status to see if they are ready to plug well and found that they have caught fish and are going back in with 1 1/2 tubing. Should be ready to plug soon.
1236019352 2003-12-11 Plug / Plug Back No Violations Check on rig to see if they are ready to plug since catching the fish. John wants to plug from 2100ft. With shot holes and not pulling the 2 7/8 . I called Rick and spoke with him about casing string and the need for multiples of shots needed to finish plug. Rick agreed that there should be several shots to insure that the cement has a place to seek hydrostatic equilibrium
1423392870 2003-12-17 Plug / Plug Back No Violations Set plug at the deepest point that could be accessed which is 2110 ft. The 4 1/2 casing which remains in well has been shot with 10 shots and the Clinton formaiton does not have a plug . The plug was then pumped thru 1 1/2 tubing . Next pulled up to 710 ft. and shot again with 10 shots and set plug to surface.Let plug set over night and plan to tag plug and grout to surface.
1788874677 2003-11-28 Plug / Plug Back No Violations Rig still fishing for casing and junk left in the hole because casing had deteriorated into pudding. They are pulling chunks out about the size of a coffee can. Should be ready to pull good casing soon.
2066517510 2003-11-06 Plug / Plug Back No Violations Still fishing for tools in hole at 124ft/.
54208147 2004-9-2 0:00:0 FR No Violations 0.70

For data sources see[8]

References